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|
Attributes | |
ACN | 306541 |
Time | |
Date | 199506 |
Day | Thu |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : mle |
State Reference | NE |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : oma |
Operator | general aviation : corporate |
Make Model Name | Chancellor 414A & C414 |
Operating Under FAR Part | Part 91 |
Flight Phase | descent : approach landing other |
Flight Plan | VFR |
Person 1 | |
Affiliation | Other |
Function | flight crew : single pilot |
Qualification | pilot : private pilot : instrument |
Experience | flight time last 90 days : 40 flight time total : 3600 flight time type : 1500 |
ASRS Report | 306541 |
Person 2 | |
Affiliation | government : faa |
Function | controller : approach |
Qualification | controller : radar |
Events | |
Anomaly | other anomaly other other spatial deviation |
Independent Detector | other flight crewa |
Resolutory Action | none taken : unable |
Consequence | other |
Supplementary | |
Primary Problem | Flight Crew Human Performance |
Air Traffic Incident | Pilot Deviation |
Narrative:
Inadvertently did not lower gear on landing. Callback conversation with reporter revealed the following: reporter stated that he had been held up too high for too long and when he broke out of the clouds he was directly over the airport. He had been on an IFR flight plan but changed airports and kept asking for lower. Instead he got a slam dunk and built up his speed so much that he delayed his gear on downwind to slow the aircraft more. On base to final he felt he must have a tailwind as the aircraft did not slow down. Of course the gear up confign was the problem. Reporter says he still wakes up at night to the sound of the propellers and skin noise as he slid down the runway. Aircraft was totalled partly because of delay in getting parts and the fact the aircraft would have been OTS for too long. FAA has given reporter remedial training for 3 hours in a 172RG.
Original NASA ASRS Text
Title: CPR PLT LANDS C414 GEAR UP.
Narrative: INADVERTENTLY DID NOT LOWER GEAR ON LNDG. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING: RPTR STATED THAT HE HAD BEEN HELD UP TOO HIGH FOR TOO LONG AND WHEN HE BROKE OUT OF THE CLOUDS HE WAS DIRECTLY OVER THE ARPT. HE HAD BEEN ON AN IFR FLT PLAN BUT CHANGED ARPTS AND KEPT ASKING FOR LOWER. INSTEAD HE GOT A SLAM DUNK AND BUILT UP HIS SPD SO MUCH THAT HE DELAYED HIS GEAR ON DOWNWIND TO SLOW THE ACFT MORE. ON BASE TO FINAL HE FELT HE MUST HAVE A TAILWIND AS THE ACFT DID NOT SLOW DOWN. OF COURSE THE GEAR UP CONFIGN WAS THE PROB. RPTR SAYS HE STILL WAKES UP AT NIGHT TO THE SOUND OF THE PROPS AND SKIN NOISE AS HE SLID DOWN THE RWY. ACFT WAS TOTALLED PARTLY BECAUSE OF DELAY IN GETTING PARTS AND THE FACT THE ACFT WOULD HAVE BEEN OTS FOR TOO LONG. FAA HAS GIVEN RPTR REMEDIAL TRAINING FOR 3 HRS IN A 172RG.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.