37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 317556 |
Time | |
Date | 199509 |
Day | Sat |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | atc facility : boy |
State Reference | WY |
Altitude | msl bound lower : 35000 msl bound upper : 35000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : zlc |
Operator | common carrier : air carrier |
Make Model Name | Commercial Fixed Wing |
Operating Under FAR Part | Part 121 |
Flight Phase | cruise other |
Route In Use | enroute : direct enroute : on vectors |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : atp pilot : flight engineer |
Experience | flight time last 90 days : 135 flight time total : 3500 flight time type : 150 |
ASRS Report | 317556 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | non adherence : clearance other spatial deviation |
Independent Detector | other controllera other flight crewa |
Resolutory Action | flight crew : became reoriented flight crew : returned to intended course or assigned course other |
Consequence | faa : reviewed incident with flight crew |
Supplementary | |
Primary Problem | Flight Crew Human Performance |
Air Traffic Incident | Pilot Deviation |
Narrative:
Captain was flying and navigating. While current ATC instructions were to 'fly heading 310 degrees until receiving mullen pass, proceed direct and continue the glasr 3 arrival into sea.' our ground track took us directly overhead which we had been using for orientation in our VOR only equipped aircraft. Frequencys of boy and mlp are the same 117.8. Upon station passage at boy, the captain thought we were overhead mlp and proceeded to turn the aircraft to 255 degrees to track the arrival. It was a gradual turn which I didn't notice because I was turned, talking with the flight engineer. Upon notice of the heading change and discussion with the captain, we turned to the correct heading of 310 degrees. ZLC asked about our heading, and gave several course corrections to get us back on the proper ground track. There were no known traffic conflicts. Because of the long flight, excellent WX and easy ATC instructions crew complacency was a major factor. This deviation also stresses the need to verbalize actions within the cockpit for effective CRM.
Original NASA ASRS Text
Title: TRACK DEV.
Narrative: CAPT WAS FLYING AND NAVING. WHILE CURRENT ATC INSTRUCTIONS WERE TO 'FLY HDG 310 DEGS UNTIL RECEIVING MULLEN PASS, PROCEED DIRECT AND CONTINUE THE GLASR 3 ARR INTO SEA.' OUR GND TRACK TOOK US DIRECTLY OVERHEAD WHICH WE HAD BEEN USING FOR ORIENTATION IN OUR VOR ONLY EQUIPPED ACFT. FREQS OF BOY AND MLP ARE THE SAME 117.8. UPON STATION PASSAGE AT BOY, THE CAPT THOUGHT WE WERE OVERHEAD MLP AND PROCEEDED TO TURN THE ACFT TO 255 DEGS TO TRACK THE ARR. IT WAS A GRADUAL TURN WHICH I DIDN'T NOTICE BECAUSE I WAS TURNED, TALKING WITH THE FE. UPON NOTICE OF THE HDG CHANGE AND DISCUSSION WITH THE CAPT, WE TURNED TO THE CORRECT HDG OF 310 DEGS. ZLC ASKED ABOUT OUR HDG, AND GAVE SEVERAL COURSE CORRECTIONS TO GET US BACK ON THE PROPER GND TRACK. THERE WERE NO KNOWN TFC CONFLICTS. BECAUSE OF THE LONG FLT, EXCELLENT WX AND EASY ATC INSTRUCTIONS CREW COMPLACENCY WAS A MAJOR FACTOR. THIS DEV ALSO STRESSES THE NEED TO VERBALIZE ACTIONS WITHIN THE COCKPIT FOR EFFECTIVE CRM.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.