37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 341846 |
Time | |
Date | 199607 |
Day | Wed |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | atc facility : phl |
State Reference | PA |
Altitude | msl bound lower : 33000 msl bound upper : 33000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : zob |
Operator | common carrier : air carrier |
Make Model Name | Commercial Fixed Wing |
Operating Under FAR Part | Part 121 |
Flight Phase | cruise other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : cfi pilot : atp pilot : flight engineer |
Experience | flight time last 90 days : 180 flight time total : 6100 flight time type : 1200 |
ASRS Report | 341846 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | none taken : unable |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
At leveloff, noticed decreasing oil quantity #2 engine. Loss rate approximately 1 quart, 3-4 mins. Talked with company. They suspected bad quantity gauge. Pressure and temperature were good. Considered pit as possible diversion airport. Continued anyway until quantity read zero. Pressure and temperature remained green arc for another 15 mins, then pressure started to fluctuate. Shut down engine, diverted to phl since it was closest, and were heavy weight 103500 pounds. Flew single engine approach, flaps 15 degrees. Landed uneventfully. Bolt head had broken off of gear box.
Original NASA ASRS Text
Title: ACFT EQUIP PROB. BROKEN GEAR BOX BOLT CAUSED LOSS OF OIL. ENG SHUTDOWN AND UNEVENTFUL SINGLE ENG LNDG.
Narrative: AT LEVELOFF, NOTICED DECREASING OIL QUANTITY #2 ENG. LOSS RATE APPROX 1 QUART, 3-4 MINS. TALKED WITH COMPANY. THEY SUSPECTED BAD QUANTITY GAUGE. PRESSURE AND TEMP WERE GOOD. CONSIDERED PIT AS POSSIBLE DIVERSION ARPT. CONTINUED ANYWAY UNTIL QUANTITY READ ZERO. PRESSURE AND TEMP REMAINED GREEN ARC FOR ANOTHER 15 MINS, THEN PRESSURE STARTED TO FLUCTUATE. SHUT DOWN ENG, DIVERTED TO PHL SINCE IT WAS CLOSEST, AND WERE HVY WT 103500 LBS. FLEW SINGLE ENG APCH, FLAPS 15 DEGS. LANDED UNEVENTFULLY. BOLT HEAD HAD BROKEN OFF OF GEAR BOX.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.