37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 357858 |
Time | |
Date | 199701 |
Day | Fri |
Local Time Of Day | 0001 To 0600 |
Place | |
Locale Reference | atc facility : dfw |
State Reference | TX |
Altitude | msl bound lower : 4000 msl bound upper : 4000 |
Environment | |
Light | Night |
Aircraft 1 | |
Controlling Facilities | tracon : dfw |
Operator | common carrier : air carrier |
Make Model Name | Commercial Fixed Wing |
Operating Under FAR Part | Part 121 |
Flight Phase | climbout : initial other |
Route In Use | departure other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : flight engineer pilot : commercial pilot : atp pilot : instrument |
Experience | flight time last 90 days : 200 flight time total : 6000 flight time type : 1000 |
ASRS Report | 357858 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : instrument |
Events | |
Anomaly | aircraft equipment problem : critical non adherence : published procedure non adherence : far other anomaly other |
Independent Detector | other flight crewa other other : unspecified cockpit |
Resolutory Action | other |
Consequence | Other |
Supplementary | |
Air Traffic Incident | Pilot Deviation |
Narrative:
Air turn-back for landing occurred due to the aircraft not pressurizing. This resulted in an unscheduled landing. Problem arose from a newly hired and inexperienced crew member not properly closing entry door (main door). An air leak caused the aircraft not to pressurize. Contributing factor may have been the flight engineer not checking that the cabin was pressurizing prior to departure. Whenever a switch is moved or a button is pushed or selector is moved and there is an associated light-or-gauge, it should be checked to assure that that system is performing the selected function. This would have led us to recognition of the problem prior to takeoff. After landing back at departure airport we solved the problem by properly relatching door, advising maintenance and operations via commercial radio, and received a new release and directive from maintenance to continue to our original destination.
Original NASA ASRS Text
Title: A LGT ACFT WAS UNABLE TO PRESSURIZE THE CABIN AFTER TKOF AND INITIAL CLB. ACFT RETURNED TO THE FIELD. FOUND MAIN ENTRANCE DOOR CLOSED BUT NOT LATCHED.
Narrative: AIR TURN-BACK FOR LNDG OCCURRED DUE TO THE ACFT NOT PRESSURIZING. THIS RESULTED IN AN UNSCHEDULED LNDG. PROB AROSE FROM A NEWLY HIRED AND INEXPERIENCED CREW MEMBER NOT PROPERLY CLOSING ENTRY DOOR (MAIN DOOR). AN AIR LEAK CAUSED THE ACFT NOT TO PRESSURIZE. CONTRIBUTING FACTOR MAY HAVE BEEN THE FE NOT CHKING THAT THE CABIN WAS PRESSURIZING PRIOR TO DEP. WHENEVER A SWITCH IS MOVED OR A BUTTON IS PUSHED OR SELECTOR IS MOVED AND THERE IS AN ASSOCIATED LIGHT-OR-GAUGE, IT SHOULD BE CHKED TO ASSURE THAT THAT SYS IS PERFORMING THE SELECTED FUNCTION. THIS WOULD HAVE LED US TO RECOGNITION OF THE PROB PRIOR TO TKOF. AFTER LNDG BACK AT DEP ARPT WE SOLVED THE PROB BY PROPERLY RELATCHING DOOR, ADVISING MAINT AND OPS VIA COMMERCIAL RADIO, AND RECEIVED A NEW RELEASE AND DIRECTIVE FROM MAINT TO CONTINUE TO OUR ORIGINAL DEST.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.