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|
Attributes | |
ACN | 363923 |
Time | |
Date | 199703 |
Day | Thu |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | airport : rsw |
State Reference | FL |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | Mixed |
Light | Night |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | MD-88 |
Operating Under FAR Part | Part 121 |
Navigation In Use | Other Other |
Flight Phase | ground : parked ground other : taxi landing other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp pilot : flight engineer |
Experience | flight time last 90 days : 190 flight time total : 9000 flight time type : 600 |
ASRS Report | 363923 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : instrument pilot : commercial |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | flight crew : overcame equipment problem other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
Upon touchdown in rsw, heard circuit breaker pop and smelled electrical fume. Dissipated when turning off runway and taxied into gate. With cockpit floods on, found digital flight guidance computer #1 circuit breaker opened. Reset with same results. Called for contract maintenance. Posted fire guard when opening east&east compartment. Everything checked ok. Maintenance tried to reset circuit breaker with same results. Aircraft was dispatched with digital flight guidance computer #1 and flight director command system #1 inoperative. This was a repeat irregularity that caused the aircraft to be removed from service earlier that day. They replaced digital flight guidance computer #1. It should also be noted that no autoplt was in use through approach and landing and that digital flight guidance computer #2 was selected since it was the first officer's leg. I'm just happy it didn't happen during the WX penetration into florida and that it wasn't a fire or smoke event. Callback conversation with reporter revealed the following information: the captain of this MD88 said that the circuit to his digital flight guidance computer was not re- established during the rest of the day. He was very critical of his company's maintenance procedure. He alleged that the maintenance personnel simply replace components without diagnosing the problem and he said that that technique led to the problem in this case.
Original NASA ASRS Text
Title: AN ACR MD88 FLC HAS THE CIRCUIT BREAKER TO THE CAPT'S DIGITAL FLT GUIDANCE COMPUTER OPEN WITH A LOUD POP AND THEY SMELLED ELECTRICAL FUMES. THIS WAS A REPEAT EVENT AND THE SYS WAS DISABLED IN ACCORDANCE WITH THE MEL.
Narrative: UPON TOUCHDOWN IN RSW, HEARD CIRCUIT BREAKER POP AND SMELLED ELECTRICAL FUME. DISSIPATED WHEN TURNING OFF RWY AND TAXIED INTO GATE. WITH COCKPIT FLOODS ON, FOUND DIGITAL FLT GUIDANCE COMPUTER #1 CIRCUIT BREAKER OPENED. RESET WITH SAME RESULTS. CALLED FOR CONTRACT MAINT. POSTED FIRE GUARD WHEN OPENING E&E COMPARTMENT. EVERYTHING CHKED OK. MAINT TRIED TO RESET CIRCUIT BREAKER WITH SAME RESULTS. ACFT WAS DISPATCHED WITH DIGITAL FLT GUIDANCE COMPUTER #1 AND FLT DIRECTOR COMMAND SYS #1 INOP. THIS WAS A REPEAT IRREGULARITY THAT CAUSED THE ACFT TO BE REMOVED FROM SVC EARLIER THAT DAY. THEY REPLACED DIGITAL FLT GUIDANCE COMPUTER #1. IT SHOULD ALSO BE NOTED THAT NO AUTOPLT WAS IN USE THROUGH APCH AND LNDG AND THAT DIGITAL FLT GUIDANCE COMPUTER #2 WAS SELECTED SINCE IT WAS THE FO'S LEG. I'M JUST HAPPY IT DIDN'T HAPPEN DURING THE WX PENETRATION INTO FLORIDA AND THAT IT WASN'T A FIRE OR SMOKE EVENT. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THE CAPT OF THIS MD88 SAID THAT THE CIRCUIT TO HIS DIGITAL FLT GUIDANCE COMPUTER WAS NOT RE- ESTABLISHED DURING THE REST OF THE DAY. HE WAS VERY CRITICAL OF HIS COMPANY'S MAINT PROC. HE ALLEGED THAT THE MAINT PERSONNEL SIMPLY REPLACE COMPONENTS WITHOUT DIAGNOSING THE PROB AND HE SAID THAT THAT TECHNIQUE LED TO THE PROB IN THIS CASE.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.