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|
Attributes | |
ACN | 398744 |
Time | |
Date | 199804 |
Day | Tue |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | atc facility : bwi |
State Reference | MD |
Altitude | msl bound lower : 1000 msl bound upper : 1000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : bwi tower : bwi |
Operator | common carrier : air carrier |
Make Model Name | B737-200 |
Operating Under FAR Part | Part 121 |
Flight Phase | climbout : takeoff other other |
Route In Use | departure other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 200 flight time total : 10000 |
ASRS Report | 398744 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : instrument pilot : commercial |
Experience | flight time last 90 days : 240 flight time total : 7000 |
ASRS Report | 398747 |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | flight crew : declared emergency other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
On takeoff after gear and flaps up and climb thrust selected, the left engine stayed at takeoff thrust and would not respond to thrust lever commands. Engine was shut down and a single engine overweight landing was accomplished uneventfully. No injuries were sustained. Callback conversation with reporter revealed the following information: the reporter stated the engine was a P&west JT8D-9 engine. The loss of engine control was caused by the fuel control unit failure. The reporter stated the thrust lever had movement but no control.
Original NASA ASRS Text
Title: A B737-200 ON TKOF AT 1000 FT DIVERTED AND SHUT DOWN #1 ENG DUE TO STAYING AT TKOF PWR CAUSED BY A FAILED FUEL CTL UNIT.
Narrative: ON TKOF AFTER GEAR AND FLAPS UP AND CLB THRUST SELECTED, THE L ENG STAYED AT TKOF THRUST AND WOULD NOT RESPOND TO THRUST LEVER COMMANDS. ENG WAS SHUT DOWN AND A SINGLE ENG OVERWT LNDG WAS ACCOMPLISHED UNEVENTFULLY. NO INJURIES WERE SUSTAINED. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THE RPTR STATED THE ENG WAS A P&W JT8D-9 ENG. THE LOSS OF ENG CTL WAS CAUSED BY THE FUEL CTL UNIT FAILURE. THE RPTR STATED THE THRUST LEVER HAD MOVEMENT BUT NO CTL.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.