37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 423103 |
Time | |
Date | 199812 |
Day | Sun |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | atc facility : dxo |
State Reference | MI |
Altitude | msl bound lower : 15000 msl bound upper : 15000 |
Environment | |
Flight Conditions | IMC |
Light | Night |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | DC-9 30 |
Flight Phase | other other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Experience | flight time last 90 days : 210 flight time total : 15000 flight time type : 2500 |
ASRS Report | 423103 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : instrument |
Experience | flight time last 90 days : 200 flight time total : 5000 flight time type : 2000 |
ASRS Report | 423323 |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa other other : unspecified |
Resolutory Action | flight crew : declared emergency other |
Consequence | Other |
Narrative:
On initial climb out at approximately 15000 ft, the cabin pressure master warning light illuminated, cabin climb rate was pegged out, followed by the cabin oxygen light and the cabin oxygen masks deploying. Engine and wing anti-ice were on and I secured both. The lead flight attendant entered the cockpit and asked for an update and almost immediately thereafter informed us there was smoke in the cabin. Declared an emergency and shot an ILS to runway 3L in dtw. No passenger evacuate/evacuation. Callback conversation with reporter revealed the following information: the reporter stated the cause of the pressure loss is unknown as no follow-up was made by the reporter. The reporter said all the emergency system, mask deployment, and passenger oxygen worked ok. Callback conversation with reporter acn 423323 revealed the following information: the reporter stated the cause of the cabin pressure loss was not known as the reporter did not follow up with maintenance on the corrective action. The reporter said the cause of the smoke could possibly have been the oxygen generators that were used. The reporter stated that on the ground no source of the smoke could be determined.
Original NASA ASRS Text
Title: A DC9-30 IN CLB AT 15000 FT DECLARED AN EMER AND DIVERTED DUE TO LOSS OF CABIN PRESSURE AND RPTED SMOKE IN THE CABIN. CAUSE OF PRESSURE LOSS UNKNOWN.
Narrative: ON INITIAL CLBOUT AT APPROX 15000 FT, THE CABIN PRESSURE MASTER WARNING LIGHT ILLUMINATED, CABIN CLB RATE WAS PEGGED OUT, FOLLOWED BY THE CABIN OXYGEN LIGHT AND THE CABIN OXYGEN MASKS DEPLOYING. ENG AND WING ANTI-ICE WERE ON AND I SECURED BOTH. THE LEAD FLT ATTENDANT ENTERED THE COCKPIT AND ASKED FOR AN UPDATE AND ALMOST IMMEDIATELY THEREAFTER INFORMED US THERE WAS SMOKE IN THE CABIN. DECLARED AN EMER AND SHOT AN ILS TO RWY 3L IN DTW. NO PAX EVAC. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THE RPTR STATED THE CAUSE OF THE PRESSURE LOSS IS UNKNOWN AS NO FOLLOW-UP WAS MADE BY THE RPTR. THE RPTR SAID ALL THE EMER SYS, MASK DEPLOYMENT, AND PAX OXYGEN WORKED OK. CALLBACK CONVERSATION WITH RPTR ACN 423323 REVEALED THE FOLLOWING INFO: THE RPTR STATED THE CAUSE OF THE CABIN PRESSURE LOSS WAS NOT KNOWN AS THE RPTR DID NOT FOLLOW UP WITH MAINT ON THE CORRECTIVE ACTION. THE RPTR SAID THE CAUSE OF THE SMOKE COULD POSSIBLY HAVE BEEN THE OXYGEN GENERATORS THAT WERE USED. THE RPTR STATED THAT ON THE GND NO SOURCE OF THE SMOKE COULD BE DETERMINED.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.