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|
Attributes | |
ACN | 439315 |
Time | |
Date | 199906 |
Day | Sun |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : pdx.airport |
State Reference | OR |
Altitude | agl single value : 0 |
Environment | |
Flight Conditions | Mixed |
Weather Elements | Rain |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tower : pdx.tower |
Operator | common carrier : air carrier |
Make Model Name | B727 Undifferentiated or Other Model |
Operating Under FAR Part | Part 121 |
Flight Phase | ground : takeoff roll |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : flight engineer pilot : atp |
Experience | flight time last 90 days : 300 flight time total : 6500 flight time type : 175 |
ASRS Report | 439315 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | other flight crewa other flight crewb |
Resolutory Action | flight crew : rejected takeoff |
Consequence | other |
Supplementary | |
Problem Areas | Aircraft Environmental Factor Maintenance Human Performance |
Primary Problem | Aircraft |
Narrative:
On initial takeoff roll the captain had trouble setting the power using the EPR gauges. I assisted and we got the EPR settings to stabilize on the bug settings. I then noticed the N1 rotor speeds all read about 85% -- normal takeoff power readings are 95%. I brought this to the captain's attention and he aborted the takeoff. Our speed had topped out at 75 KTS during our initial roll. We returned to the ramp and wrote up the anomalous engine readings. The next day our mechanics told us they had removed a large amount of insects and related material from the tubes and lines associated with the probes that provide the pressure readings for the EPR gauges. We also found out at that point that the airplane had sat several days without engine covers or plugs. I believe this whole incident could have been avoided if procedures regarding long-term aircraft parking had been followed.
Original NASA ASRS Text
Title: B727 LOW SPD ABORT AT PDX.
Narrative: ON INITIAL TKOF ROLL THE CAPT HAD TROUBLE SETTING THE PWR USING THE EPR GAUGES. I ASSISTED AND WE GOT THE EPR SETTINGS TO STABILIZE ON THE BUG SETTINGS. I THEN NOTICED THE N1 ROTOR SPDS ALL READ ABOUT 85% -- NORMAL TKOF PWR READINGS ARE 95%. I BROUGHT THIS TO THE CAPT'S ATTN AND HE ABORTED THE TKOF. OUR SPD HAD TOPPED OUT AT 75 KTS DURING OUR INITIAL ROLL. WE RETURNED TO THE RAMP AND WROTE UP THE ANOMALOUS ENG READINGS. THE NEXT DAY OUR MECHS TOLD US THEY HAD REMOVED A LARGE AMOUNT OF INSECTS AND RELATED MATERIAL FROM THE TUBES AND LINES ASSOCIATED WITH THE PROBES THAT PROVIDE THE PRESSURE READINGS FOR THE EPR GAUGES. WE ALSO FOUND OUT AT THAT POINT THAT THE AIRPLANE HAD SAT SEVERAL DAYS WITHOUT ENG COVERS OR PLUGS. I BELIEVE THIS WHOLE INCIDENT COULD HAVE BEEN AVOIDED IF PROCS REGARDING LONG-TERM ACFT PARKING HAD BEEN FOLLOWED.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.