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|
Attributes | |
ACN | 465208 |
Time | |
Date | 200003 |
Day | Sun |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : pbi.airport |
State Reference | FL |
Altitude | msl single value : 14500 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : zma.artcc |
Operator | common carrier : air carrier |
Make Model Name | MD-80 Series (DC-9-80) Undifferentiated or Other Model |
Operating Under FAR Part | Part 121 |
Flight Phase | climbout : intermediate altitude |
Route In Use | enroute : on vectors |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 180 flight time total : 11500 flight time type : 5000 |
ASRS Report | 465208 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : instrument pilot : commercial pilot : multi engine |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other anomaly other anomaly other |
Independent Detector | other flight crewa other flight crewb |
Resolutory Action | flight crew : diverted to another airport flight crew : declared emergency |
Consequence | other |
Supplementary | |
Problem Areas | Aircraft |
Primary Problem | Aircraft |
Narrative:
On climb at approximately 14500 ft, white smoke was detected in the cockpit. Both the first officer and I donned our oxygen masks immediately. The intensity of the smoke was increasing. I disconnected the autoplt and autothrottles and turned back towards pbi. The first officer had trouble establishing contact with ATC. I was able to communicate with ZMA and demand a return to the nearest airport. I initially requested direct fll then realized pbi was closer and was cleared direct pbi. The first officer started the checklist for interior fire/smoke. The L1 flight attendant then entered the cockpit to tell us about the 'mist' in the cabin. I told her we were returning to pbi. I was descending at approximately 335 KIAS direct the pbi VOR. I then made a quick PA to passenger. We contacted pbi approach control and cleared for the visual runway 27R. At this time the smoke was gone and the first officer and I removed our oxygen masks. I informed ATC the smoke was now gone, but requested the emergency equipment would meet us. The first officer and I completed the descent/approach and landing checklists and made a normal landing. Our landing weight was approximately 13500 pounds (making us overweight). After speaking with the tower controller and directly to the fire trucks, I was assured there was no fire or smoke in or around the aircraft. I made a brief PA to the passenger and then taxied to the gate and the passenger deplaned through the jetway. No damage to the aircraft and no injuries to passenger. The cause of the smoke was determined to be an oil leak in the APU allowing a small amount of oil into the air conditioning system. The problem was fixed, an overweight landing inspection completed and although 4 hours late, we completed the flight to lga.
Original NASA ASRS Text
Title: MD80 RETURNS TO PBI, FL, FOR SMOKE IN THE COCKPIT.
Narrative: ON CLB AT APPROX 14500 FT, WHITE SMOKE WAS DETECTED IN THE COCKPIT. BOTH THE FO AND I DONNED OUR OXYGEN MASKS IMMEDIATELY. THE INTENSITY OF THE SMOKE WAS INCREASING. I DISCONNECTED THE AUTOPLT AND AUTOTHROTTLES AND TURNED BACK TOWARDS PBI. THE FO HAD TROUBLE ESTABLISHING CONTACT WITH ATC. I WAS ABLE TO COMMUNICATE WITH ZMA AND DEMAND A RETURN TO THE NEAREST ARPT. I INITIALLY REQUESTED DIRECT FLL THEN REALIZED PBI WAS CLOSER AND WAS CLRED DIRECT PBI. THE FO STARTED THE CHKLIST FOR INTERIOR FIRE/SMOKE. THE L1 FLT ATTENDANT THEN ENTERED THE COCKPIT TO TELL US ABOUT THE 'MIST' IN THE CABIN. I TOLD HER WE WERE RETURNING TO PBI. I WAS DSNDING AT APPROX 335 KIAS DIRECT THE PBI VOR. I THEN MADE A QUICK PA TO PAX. WE CONTACTED PBI APCH CTL AND CLRED FOR THE VISUAL RWY 27R. AT THIS TIME THE SMOKE WAS GONE AND THE FO AND I REMOVED OUR OXYGEN MASKS. I INFORMED ATC THE SMOKE WAS NOW GONE, BUT REQUESTED THE EMER EQUIP WOULD MEET US. THE FO AND I COMPLETED THE DSCNT/APCH AND LNDG CHKLISTS AND MADE A NORMAL LNDG. OUR LNDG WT WAS APPROX 13500 LBS (MAKING US OVERWT). AFTER SPEAKING WITH THE TWR CTLR AND DIRECTLY TO THE FIRE TRUCKS, I WAS ASSURED THERE WAS NO FIRE OR SMOKE IN OR AROUND THE ACFT. I MADE A BRIEF PA TO THE PAX AND THEN TAXIED TO THE GATE AND THE PAX DEPLANED THROUGH THE JETWAY. NO DAMAGE TO THE ACFT AND NO INJURIES TO PAX. THE CAUSE OF THE SMOKE WAS DETERMINED TO BE AN OIL LEAK IN THE APU ALLOWING A SMALL AMOUNT OF OIL INTO THE AIR CONDITIONING SYS. THE PROB WAS FIXED, AN OVERWT LNDG INSPECTION COMPLETED AND ALTHOUGH 4 HRS LATE, WE COMPLETED THE FLT TO LGA.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.