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|
Attributes | |
ACN | 493737 |
Time | |
Date | 200011 |
Day | Mon |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : lsf.airport |
State Reference | GA |
Altitude | msl single value : 3500 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | military facility : lsf.milfac tracon : csg.tracon |
Operator | general aviation : instructional |
Make Model Name | Duchess 76 |
Operating Under FAR Part | Part 91 |
Navigation In Use | other vortac |
Flight Phase | cruise : level |
Route In Use | enroute : on vectors |
Flight Plan | IFR |
Person 1 | |
Affiliation | other |
Function | instruction : trainee |
Qualification | pilot : private pilot : instrument |
Experience | flight time last 90 days : 22 flight time total : 290 flight time type : 23 |
ASRS Report | 493737 |
Person 2 | |
Affiliation | other |
Function | instruction : instructor |
Qualification | pilot : cfi pilot : multi engine |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | other flight crewa other flight crewb |
Resolutory Action | controller : issued new clearance flight crew : landed in emergency condition flight crew : declared emergency |
Consequence | faa : reviewed incident with flight crew other |
Supplementary | |
Problem Areas | Aircraft |
Primary Problem | Aircraft |
Narrative:
All normal procedures for operating the aircraft took place. Checklists were used for all procedures. Preflight inspection was properly done with no evidence of anything inoperative. Fuel and oil were checked and both were to their normal operating ranges. Flight was departed to the east and I opened my flight plan for my check ride with an official instructor. Approximately 25 mins into the training flight, the right engine lost power. With the aid of the instructor, we tried to troubleshoot the problem. Fuel pressure was at zero, and auxiliary pump was activated. Engine power was regained for 15-20 seconds and then quit. Notifying the ATC controller, an emergency was declared as the left engine also quit momentarily. The left engine sputtered once more before landing. Power was available during landing and the left engine was immediately shut down after touchdown. Loss of fuel is evident to the cause of incident. Further investigation is needed for verification.
Original NASA ASRS Text
Title: A BE76 STUDENT PLT RPTED AN ENG FAILURE NW OF LSF.
Narrative: ALL NORMAL PROCS FOR OPERATING THE ACFT TOOK PLACE. CHKLISTS WERE USED FOR ALL PROCS. PREFLT INSPECTION WAS PROPERLY DONE WITH NO EVIDENCE OF ANYTHING INOP. FUEL AND OIL WERE CHKED AND BOTH WERE TO THEIR NORMAL OPERATING RANGES. FLT WAS DEPARTED TO THE E AND I OPENED MY FLT PLAN FOR MY CHK RIDE WITH AN OFFICIAL INSTRUCTOR. APPROX 25 MINS INTO THE TRAINING FLT, THE R ENG LOST PWR. WITH THE AID OF THE INSTRUCTOR, WE TRIED TO TROUBLESHOOT THE PROB. FUEL PRESSURE WAS AT ZERO, AND AUX PUMP WAS ACTIVATED. ENG PWR WAS REGAINED FOR 15-20 SECONDS AND THEN QUIT. NOTIFYING THE ATC CTLR, AN EMER WAS DECLARED AS THE L ENG ALSO QUIT MOMENTARILY. THE L ENG SPUTTERED ONCE MORE BEFORE LNDG. PWR WAS AVAILABLE DURING LNDG AND THE L ENG WAS IMMEDIATELY SHUT DOWN AFTER TOUCHDOWN. LOSS OF FUEL IS EVIDENT TO THE CAUSE OF INCIDENT. FURTHER INVESTIGATION IS NEEDED FOR VERIFICATION.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.