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|
Attributes | |
ACN | 506630 |
Time | |
Date | 200103 |
Day | Thu |
Place | |
Locale Reference | airport : msp.airport |
State Reference | MN |
Altitude | msl single value : 6000 |
Environment | |
Flight Conditions | IMC |
Light | Night |
Aircraft 1 | |
Operator | general aviation : personal |
Make Model Name | Small Aircraft, High Wing, 1 Eng, Fixed Gear |
Flight Phase | descent : approach |
Route In Use | arrival : on vectors |
Flight Plan | IFR |
Person 1 | |
Affiliation | other |
Function | flight crew : single pilot |
Qualification | pilot : commercial pilot : instrument |
Experience | flight time last 90 days : 25 flight time total : 4630 flight time type : 1850 |
ASRS Report | 506630 |
Events | |
Anomaly | aircraft equipment problem : critical altitude deviation : overshoot altitude deviation : excursion from assigned altitude non adherence : far non adherence : clearance non adherence : published procedure other spatial deviation |
Resolutory Action | controller : issued alert controller : issued new clearance |
Supplementary | |
Problem Areas | Aircraft Flight Crew Human Performance |
Primary Problem | Flight Crew Human Performance |
Air Traffic Incident | Pilot Deviation |
Narrative:
I received approach instructions for a descent in IMC. While descending on the vectored heading I was reviewing the approach procedure to the alternate airport. A loud noise suddenly occurred when the oil filler door broke open and caused distraction. After the source of the noise was determined I accidentally deviated from clearance instructions by flying directly to gep VOR before reaching the assigned altitude for the turn. Approach brought the deviation to my attention and issued new instructions. The rest of the approach was uneventful until I was flying at MDA looking for the runway. I inadvertently dropped below MDA and an altitude alert was issued by the tower. Shortly after that the runway came in sight and I landed. I believe fatigue played a major role in this event. I worked late the night before and then got up early to finish some tasks before I could leave. I was flying for about 6 hours before starting the approach.
Original NASA ASRS Text
Title: SMA PLT HAD AN ALTDEV AND TRACK DEV.
Narrative: I RECEIVED APCH INSTRUCTIONS FOR A DSCNT IN IMC. WHILE DSNDING ON THE VECTORED HEADING I WAS REVIEWING THE APCH PROC TO THE ALTERNATE ARPT. A LOUD NOISE SUDDENLY OCCURRED WHEN THE OIL FILLER DOOR BROKE OPEN AND CAUSED DISTR. AFTER THE SOURCE OF THE NOISE WAS DETERMINED I ACCIDENTALLY DEVIATED FROM CLRNC INSTRUCTIONS BY FLYING DIRECTLY TO GEP VOR BEFORE REACHING THE ASSIGNED ALT FOR THE TURN. APCH BROUGHT THE DEV TO MY ATTN AND ISSUED NEW INSTRUCTIONS. THE REST OF THE APCH WAS UNEVENTFUL UNTIL I WAS FLYING AT MDA LOOKING FOR THE RWY. I INADVERTENTLY DROPPED BELOW MDA AND AN ALT ALERT WAS ISSUED BY THE TWR. SHORTLY AFTER THAT THE RWY CAME IN SIGHT AND I LANDED. I BELIEVE FATIGUE PLAYED A MAJOR ROLE IN THIS EVENT. I WORKED LATE THE NIGHT BEFORE AND THEN GOT UP EARLY TO FINISH SOME TASKS BEFORE I COULD LEAVE. I WAS FLYING FOR ABOUT 6 HRS BEFORE STARTING THE APCH.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.