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|
Attributes | |
ACN | 549047 |
Time | |
Date | 200205 |
Day | Thu |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : dfw.airport |
State Reference | TX |
Altitude | msl single value : 10000 |
Environment | |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : d10.tracon tower : lch.tower |
Operator | common carrier : air carrier |
Make Model Name | MD-80 Super 80 |
Operating Under FAR Part | Part 121 |
Navigation In Use | other |
Flight Phase | climbout : intermediate altitude |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
ASRS Report | 549047 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | aircraft equipment other aircraft equipment : cabin pressure indicator other flight crewa other flight crewb other other : fa 3 |
Resolutory Action | flight crew : declared emergency flight crew : landed in emergency condition flight crew : diverted to another airport |
Consequence | other other |
Supplementary | |
Problem Areas | Aircraft |
Primary Problem | Aircraft |
Narrative:
Departed dfw with right air conditioning pack placarded inoperative. After takeoff, aircraft would not pressurize. Followed operations manual procedures -- no help. Flight attendant reported loud air noise from rear of aircraft. Cabin temperature became uncomfortably warm. Considering these and previous problems with aircraft, I opted to exercise emergency authority/authorized and return for overweight landing at 133600 pounds. Landing was smooth and uneventful.
Original NASA ASRS Text
Title: AN MD80 CREW, DEPARTING DFW, WERE UNABLE TO PRESSURIZE THE ACFT. A RETURN TO DFW WAS INITIATED, LNDG OVERWT.
Narrative: DEPARTED DFW WITH R AIR CONDITIONING PACK PLACARDED INOP. AFTER TKOF, ACFT WOULD NOT PRESSURIZE. FOLLOWED OPS MANUAL PROCS -- NO HELP. FLT ATTENDANT RPTED LOUD AIR NOISE FROM REAR OF ACFT. CABIN TEMP BECAME UNCOMFORTABLY WARM. CONSIDERING THESE AND PREVIOUS PROBS WITH ACFT, I OPTED TO EXERCISE EMER AUTH AND RETURN FOR OVERWT LNDG AT 133600 LBS. LNDG WAS SMOOTH AND UNEVENTFUL.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.