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|
Attributes | |
ACN | 613777 |
Time | |
Date | 200403 |
Day | Wed |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | airport : iah.airport |
State Reference | TX |
Aircraft 1 | |
Controlling Facilities | tracon : i90.tracon tower : iah.tower |
Operator | common carrier : air carrier |
Make Model Name | MD-80 Series (DC-9-80) Undifferentiated or Other Model |
Operating Under FAR Part | Part 121 |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 5000 flight time total : 26000 flight time type : 230 |
ASRS Report | 613777 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : multi engine pilot : instrument pilot : commercial |
Experience | flight time last 90 days : 210 flight time total : 19000 flight time type : 210 |
ASRS Report | 613776 |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other anomaly |
Independent Detector | aircraft equipment other aircraft equipment : rt hydsystem pressure other flight crewa other flight crewb other other : 3 |
Resolutory Action | aircraft : evacuated controller : issued new clearance flight crew : declared emergency flight crew : landed in emergency condition |
Consequence | other other |
Supplementary | |
Problem Areas | Aircraft |
Primary Problem | Aircraft |
Narrative:
The event was a successful emergency evacuate/evacuation of passenger. The cause was from hydraulic smoke fumes coming into the cabin after aircraft was stopped. The right hydraulic system failed 1 hour into the flight. The crew performed the abnormal checklist and planned for all possible scenarios upon our arrival at iah. The cockpit crew formulated a plan and briefed the flight attendants on the potential events that may unfold on arrival/landing and ask that they prepare themselves for each scenario, including an evacuate/evacuation. Our plan was to begin confign early to allow time for the possibility of manually extending the landing gear in the event the right hydraulic system remaining fluid/pressure failed. Coordination 1+30 out of iah was made with ATC for runway selection and possibility of stopping on runway to secure gear and doors. Coordination with maintenance was accomplished as well. The manual gear extension procedure was performed after initial effort failed due to right system malfunction. Checklists were accomplished, flight attendants informed that we would stop on runway for gear pin installation and an emergency was declared with iah approach control. Landing was uneventful and aircraft stopped on runway. I was talking with maintenance supervisor on ground to cockpit interphone when the flight attendant informed the first officer that smoke was filling the cabin. The decision was made to evacuate/evacuation the aircraft. The announcement was made to the passenger and the first officer completed the evacuate/evacuation checklist. Supplemental information from acn 613776: flight attendant called and said we had lots of smoke in cabin. Captain ordered evacuate/evacuation. Communication and briefing with all concerned ended with successful evolution with no injuries.
Original NASA ASRS Text
Title: MD80 CREW LOST THE R HYD SYS. THE ACFT WAS EVACED AFTER LNDG AFTER HYD SMOKE ENTERED THE CABIN.
Narrative: THE EVENT WAS A SUCCESSFUL EMER EVAC OF PAX. THE CAUSE WAS FROM HYD SMOKE FUMES COMING INTO THE CABIN AFTER ACFT WAS STOPPED. THE R HYD SYS FAILED 1 HR INTO THE FLT. THE CREW PERFORMED THE ABNORMAL CHKLIST AND PLANNED FOR ALL POSSIBLE SCENARIOS UPON OUR ARR AT IAH. THE COCKPIT CREW FORMULATED A PLAN AND BRIEFED THE FLT ATTENDANTS ON THE POTENTIAL EVENTS THAT MAY UNFOLD ON ARR/LNDG AND ASK THAT THEY PREPARE THEMSELVES FOR EACH SCENARIO, INCLUDING AN EVAC. OUR PLAN WAS TO BEGIN CONFIGN EARLY TO ALLOW TIME FOR THE POSSIBILITY OF MANUALLY EXTENDING THE LNDG GEAR IN THE EVENT THE R HYD SYS REMAINING FLUID/PRESSURE FAILED. COORD 1+30 OUT OF IAH WAS MADE WITH ATC FOR RWY SELECTION AND POSSIBILITY OF STOPPING ON RWY TO SECURE GEAR AND DOORS. COORD WITH MAINT WAS ACCOMPLISHED AS WELL. THE MANUAL GEAR EXTENSION PROC WAS PERFORMED AFTER INITIAL EFFORT FAILED DUE TO R SYS MALFUNCTION. CHKLISTS WERE ACCOMPLISHED, FLT ATTENDANTS INFORMED THAT WE WOULD STOP ON RWY FOR GEAR PIN INSTALLATION AND AN EMER WAS DECLARED WITH IAH APCH CTL. LNDG WAS UNEVENTFUL AND ACFT STOPPED ON RWY. I WAS TALKING WITH MAINT SUPVR ON GND TO COCKPIT INTERPHONE WHEN THE FLT ATTENDANT INFORMED THE FO THAT SMOKE WAS FILLING THE CABIN. THE DECISION WAS MADE TO EVAC THE ACFT. THE ANNOUNCEMENT WAS MADE TO THE PAX AND THE FO COMPLETED THE EVAC CHKLIST. SUPPLEMENTAL INFO FROM ACN 613776: FLT ATTENDANT CALLED AND SAID WE HAD LOTS OF SMOKE IN CABIN. CAPT ORDERED EVAC. COM AND BRIEFING WITH ALL CONCERNED ENDED WITH SUCCESSFUL EVOLUTION WITH NO INJURIES.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.