37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 640031 |
Time | |
Date | 200402 |
Day | Sun |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | airport : zzz.airport |
State Reference | US |
Altitude | msl single value : 12000 |
Aircraft 1 | |
Controlling Facilities | tracon : zzz.tracon |
Operator | common carrier : air carrier |
Make Model Name | B737-300 |
Operating Under FAR Part | Part 121 |
Flight Phase | descent : holding |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain |
ASRS Report | 640031 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Experience | flight time last 90 days : 60 flight time total : 11000 flight time type : 3000 |
ASRS Report | 640032 |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other anomaly |
Independent Detector | other other : 3 |
Resolutory Action | controller : issued new clearance flight crew : declared emergency flight crew : diverted to another airport |
Consequence | other other |
Supplementary | |
Problem Areas | Aircraft Flight Crew Human Performance |
Primary Problem | Aircraft |
Narrative:
In holding at ZZZ, captain and first officer both smelled faint but obvious odor of smoke. Shortly thereafter, we heard flight attendant call buttons going off in cabin and shortly after that the 'a' flight attendant reported via interphone that passenger smelled smoke and so did she. There was no visible smoke. Flight attendants inspected cabin including lavatories thoroughly finding no evidence of fire or visible smoke. The captain informed center that we smelled smoke in the cabin and queried if we would be able to get into ZZZ since the reason for the hold was not known by crew. Center immediately cleared us direct to ZZZ and we set up for ILS to runway 26R, declaring an emergency. In the process of setting up, the flight attendant reported that the smell had subsided. Approach switched runway to runway 26L. Although busy, it was an expeditious approach with ATC priority and an uneventful landing. We exited runway, stopped, and had a visual inspection from airport fire equipment -- no problems seen. We taxied to gate and deplaned. Fire and maintenance inspected the aircraft and found nothing in the cabin. First officer heard loud noise from forward cargo bay on outside inspection, subsequently found by maintenance to be a faulty equipment cooling fan. It was inoperative'ed, and deferred. We flew the aircraft next leg to ord without incident. Flight attendants did excellent job of controling a somewhat panicky passenger during the event, as well as communicating with the cockpit and preparing for the quick landing. Callback conversation with reporter revealed the following information: captain stated there really was no smoke visible but mainly a burning electrical odor. The east&east compartment cooling fan had failed and no circuit breakers were found tripped. Fan was found at the diversion station by the first officer on the walkaround check and inspected by maintenance and then deferred per the MEL.
Original NASA ASRS Text
Title: A B737-300 HOLDING AT 12000 FT DECLARED AN EMER AND DIVERTED DUE TO CABIN ATTENDANT RPT OF ELECTRICAL BURNING ODOR. CAUSED BY FAILED COOLING FAN.
Narrative: IN HOLDING AT ZZZ, CAPT AND FO BOTH SMELLED FAINT BUT OBVIOUS ODOR OF SMOKE. SHORTLY THEREAFTER, WE HEARD FLT ATTENDANT CALL BUTTONS GOING OFF IN CABIN AND SHORTLY AFTER THAT THE 'A' FLT ATTENDANT RPTED VIA INTERPHONE THAT PAX SMELLED SMOKE AND SO DID SHE. THERE WAS NO VISIBLE SMOKE. FLT ATTENDANTS INSPECTED CABIN INCLUDING LAVATORIES THOROUGHLY FINDING NO EVIDENCE OF FIRE OR VISIBLE SMOKE. THE CAPT INFORMED CTR THAT WE SMELLED SMOKE IN THE CABIN AND QUERIED IF WE WOULD BE ABLE TO GET INTO ZZZ SINCE THE REASON FOR THE HOLD WAS NOT KNOWN BY CREW. CTR IMMEDIATELY CLRED US DIRECT TO ZZZ AND WE SET UP FOR ILS TO RWY 26R, DECLARING AN EMER. IN THE PROCESS OF SETTING UP, THE FLT ATTENDANT RPTED THAT THE SMELL HAD SUBSIDED. APCH SWITCHED RWY TO RWY 26L. ALTHOUGH BUSY, IT WAS AN EXPEDITIOUS APCH WITH ATC PRIORITY AND AN UNEVENTFUL LNDG. WE EXITED RWY, STOPPED, AND HAD A VISUAL INSPECTION FROM ARPT FIRE EQUIP -- NO PROBS SEEN. WE TAXIED TO GATE AND DEPLANED. FIRE AND MAINT INSPECTED THE ACFT AND FOUND NOTHING IN THE CABIN. FO HEARD LOUD NOISE FROM FORWARD CARGO BAY ON OUTSIDE INSPECTION, SUBSEQUENTLY FOUND BY MAINT TO BE A FAULTY EQUIP COOLING FAN. IT WAS INOP'ED, AND DEFERRED. WE FLEW THE ACFT NEXT LEG TO ORD WITHOUT INCIDENT. FLT ATTENDANTS DID EXCELLENT JOB OF CTLING A SOMEWHAT PANICKY PAX DURING THE EVENT, AS WELL AS COMMUNICATING WITH THE COCKPIT AND PREPARING FOR THE QUICK LNDG. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: CAPT STATED THERE REALLY WAS NO SMOKE VISIBLE BUT MAINLY A BURNING ELECTRICAL ODOR. THE E&E COMPARTMENT COOLING FAN HAD FAILED AND NO CIRCUIT BREAKERS WERE FOUND TRIPPED. FAN WAS FOUND AT THE DIVERSION STATION BY THE FO ON THE WALKAROUND CHK AND INSPECTED BY MAINT AND THEN DEFERRED PER THE MEL.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.