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|
Attributes | |
ACN | 867971 |
Time | |
Date | 200912 |
Local Time Of Day | 1801-2400 |
Place | |
Locale Reference | ZZZ.Airport |
State Reference | US |
Environment | |
Light | Night |
Aircraft 1 | |
Make Model Name | MD-83 |
Operating Under FAR Part | Part 121 |
Flight Phase | Climb |
Flight Plan | IFR |
Component | |
Aircraft Component | Nose Gear |
Person 1 | |
Function | Captain Pilot Not Flying |
Events | |
Anomaly | Aircraft Equipment Problem Critical |
Narrative:
After takeoff nose gear failed to retract. Completed MD80 'land abnormal red gear light in flight with gear handle up' checklist. Noise was loud and we climbed out at 210 KIAS to ensure we did not overspeed flaps or gear. After we completed the abnormal procedure the gear still would not retract. We declared an emergency. In the maintenance logbook there was a maintenance discrepancy that indicated a problem with the nose gear strut that was signed off. We also noticed the nose gear in-flight/ground shift mechanism was not operating on the ground properly because the strobe lights were on at the gate. Later the aircraft settled and the shift mechanism went back to ground mode. During our malfunction; this mechanism shifted to ground mode while we were in-flight. It is of my opinion this incident could have been prevented if the maintenance action had correctly diagnosed what was described as unusual noise from the nose gear during taxi. We landed without incident and maintenance said the strut had collapsed and the airplane was removed from service.
Original NASA ASRS Text
Title: An MD-80 Captain reported the nose gear failed to retract after departure. The crew subsequently declared an emergency and returned to the departure airport; the nose gear had been written up and signed off prior to departure.
Narrative: After takeoff nose gear failed to retract. Completed MD80 'Land Abnormal Red Gear Light in Flight with Gear Handle Up' checklist. Noise was loud and we climbed out at 210 KIAS to ensure we did not overspeed flaps or gear. After we completed the abnormal procedure the gear still would not retract. We declared an emergency. In the maintenance logbook there was a maintenance discrepancy that indicated a problem with the nose gear strut that was signed off. We also noticed the nose gear in-flight/ground shift mechanism was not operating on the ground properly because the strobe lights were on at the gate. Later the aircraft settled and the shift mechanism went back to ground mode. During our malfunction; this mechanism shifted to ground mode while we were in-flight. It is of my opinion this incident could have been prevented if the maintenance action had correctly diagnosed what was described as unusual noise from the nose gear during taxi. We landed without incident and Maintenance said the strut had collapsed and the airplane was removed from service.
Data retrieved from NASA's ASRS site as of April 2012 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.