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|
Attributes | |
ACN | 947520 |
Time | |
Date | 201001 |
Local Time Of Day | 1201-1800 |
Place | |
Locale Reference | ZZZ.Airport |
State Reference | US |
Environment | |
Light | Daylight |
Aircraft 1 | |
Make Model Name | B757-200 |
Operating Under FAR Part | Part 121 |
Flight Phase | Parked |
Component | |
Aircraft Component | Turbine Assembly |
Person 1 | |
Function | Technician |
Qualification | Maintenance Airframe Maintenance Powerplant |
Experience | Maintenance Technician 23 |
Events | |
Anomaly | Aircraft Equipment Problem Critical Deviation - Procedural Published Material / Policy |
Narrative:
I was working in the pratt-whitney (pw) engine stall when I was approached by the pw-2000 manager. He said he needed to speak to me about something and he went to get my supervisor. At that time I went and found my union shop steward. We both went to the supervisor's office and met with the manager and supervisor. They both informed us there was a [company] investigation being conducted on a pw-2000 engine which I had worked on over a year ago. It was explained that the engine was found to have very high oil consumption and after 1;400 hours of service [the engine] had been removed from the aircraft and taken out of service. Upon closer inspection of the number 5 bearing compartment; it was discovered that the number 5 bearing cover plate was not installed. The manager informed me that I was the mechanic who signed-off the job card.
Original NASA ASRS Text
Title: An Engine Shop Mechanic reports about a Pratt-Whitney PW-2000 engine that was removed from a B757-200 aircraft after 1400 hours of service for high oil consumption. The number 5 bearing compartment cover was found missing; but speculation about improper maintenance at line stations contributing to the missing cover was also noted.
Narrative: I was working in the Pratt-Whitney (PW) engine stall when I was approached by the PW-2000 Manager. He said he needed to speak to me about something and he went to get my Supervisor. At that time I went and found my Union Shop Steward. We both went to the Supervisor's office and met with the Manager and Supervisor. They both informed us there was a [company] investigation being conducted on a PW-2000 engine which I had worked on over a year ago. It was explained that the engine was found to have very high oil consumption and after 1;400 hours of service [the engine] had been removed from the aircraft and taken out of service. Upon closer inspection of the number 5 bearing compartment; it was discovered that the number 5 bearing cover plate was not installed. The Manager informed me that I was the Mechanic who signed-off the Job Card.
Data retrieved from NASA's ASRS site as of April 2012 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.