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|
Attributes | |
ACN | 103705 |
Time | |
Date | 198902 |
Day | Mon |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | airport : shv |
State Reference | LA |
Altitude | msl bound lower : 1000 msl bound upper : 1000 |
Environment | |
Flight Conditions | VMC |
Light | Night |
Aircraft 1 | |
Controlling Facilities | tower : shv artcc : zfw |
Operator | common carrier : air carrier |
Make Model Name | Large Transport, Low Wing, 3 Turbojet Eng |
Flight Phase | climbout : intermediate altitude |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : flight engineer pilot : instrument pilot : commercial pilot : atp |
Experience | flight time last 90 days : 120 flight time total : 3200 flight time type : 19 |
ASRS Report | 103705 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : declared emergency none taken : unable none taken : anomaly accepted |
Consequence | other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
Conducted a normal power takeoff from runway 32 at shv. At 1000' MSL we felt a big compressor stall. Engine began to spool down and egt rose rapidly. We then conducted an engine shutdown and the captain made an uneventful landing back at shv. Emergency vehicles were standing by but were not utilized. Callback conversation with reporter revealed the following: the #3 engine failed and post-flight inspection revealed compressor blade damage necessitating an engine change. Company suggested an ASRS report be filed.
Original NASA ASRS Text
Title: ACR LGT ENGINE FAILURE SHUTDOWN AFTER TKOF FROM SHV. RETURN LAND.
Narrative: CONDUCTED A NORMAL PWR TKOF FROM RWY 32 AT SHV. AT 1000' MSL WE FELT A BIG COMPRESSOR STALL. ENG BEGAN TO SPOOL DOWN AND EGT ROSE RAPIDLY. WE THEN CONDUCTED AN ENG SHUTDOWN AND THE CAPT MADE AN UNEVENTFUL LNDG BACK AT SHV. EMER VEHICLES WERE STANDING BY BUT WERE NOT UTILIZED. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING: THE #3 ENG FAILED AND POST-FLT INSPECTION REVEALED COMPRESSOR BLADE DAMAGE NECESSITATING AN ENG CHANGE. COMPANY SUGGESTED AN ASRS RPT BE FILED.
Data retrieved from NASA's ASRS site as of August 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.