37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 200514 |
Time | |
Date | 199112 |
Day | Tue |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | atc facility : zab |
State Reference | NM |
Altitude | msl bound lower : 37000 msl bound upper : 37000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : zab |
Operator | common carrier : air carrier |
Make Model Name | Medium Large Transport, Low Wing, 2 Turbojet Eng |
Navigation In Use | Other Other |
Flight Phase | cruise other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : cfi pilot : atp pilot : instrument |
Experience | flight time last 90 days : 230 flight time total : 9500 flight time type : 510 |
ASRS Report | 200514 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : less severe other anomaly |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : overcame equipment problem |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
Climbing to FL370, autoplt #2 and autothrust system engaged and active. Level off maneuver was normal, however, speed bug rapidly (approximately 1 second) decreased from approximately .755 mach to below predicted stall. Autothrust system reduced engine power to idle. No ECAM warning or messages appeared. PF deselected managed speed to selected speed and then immediately reselected managed speed. Target airspeed immediately returned to normal (approximately .75 M) and autothrust responded normally. Total anomaly and restoration to normal function took less than 10 seconds and less than 10 KTS of airspeed were lost during the power reduction to idle. Maintenance notified at destination. No failures discovered.
Original NASA ASRS Text
Title: AIRSPD DEV WHILE ACR MLG IS ON AUTOPLT AND AUTO THRUST SENSES A SPD DECREASE COMMAND THROUGH THE FMC SYS.
Narrative: CLBING TO FL370, AUTOPLT #2 AND AUTOTHRUST SYS ENGAGED AND ACTIVE. LEVEL OFF MANEUVER WAS NORMAL, HOWEVER, SPD BUG RAPIDLY (APPROX 1 SECOND) DECREASED FROM APPROX .755 MACH TO BELOW PREDICTED STALL. AUTOTHRUST SYS REDUCED ENG PWR TO IDLE. NO ECAM WARNING OR MESSAGES APPEARED. PF DESELECTED MANAGED SPD TO SELECTED SPD AND THEN IMMEDIATELY RESELECTED MANAGED SPD. TARGET AIRSPD IMMEDIATELY RETURNED TO NORMAL (APPROX .75 M) AND AUTOTHRUST RESPONDED NORMALLY. TOTAL ANOMALY AND RESTORATION TO NORMAL FUNCTION TOOK LESS THAN 10 SECONDS AND LESS THAN 10 KTS OF AIRSPD WERE LOST DURING THE PWR REDUCTION TO IDLE. MAINT NOTIFIED AT DEST. NO FAILURES DISCOVERED.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.