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|
Attributes | |
ACN | 250162 |
Time | |
Date | 199308 |
Day | Sat |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | atc facility : mkc |
State Reference | MO |
Altitude | msl bound lower : 33000 msl bound upper : 33000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : zkc |
Operator | common carrier : air carrier |
Make Model Name | Medium Large Transport, Low Wing, 2 Turbojet Eng |
Flight Phase | cruise other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : flight engineer pilot : instrument pilot : private pilot : atp |
Experience | flight time last 90 days : 150 flight time total : 10850 flight time type : 150 |
ASRS Report | 250162 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : cfi pilot : atp |
Experience | flight time last 90 days : 120 flight time total : 14000 flight time type : 10000 |
ASRS Report | 250082 |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | flight crew : declared emergency other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
Between tul and mkc, the CSD oil pressure low light came on. We verified and did the checklist which said to disconnect CSD. After trying to disconnect CSD, without any luck, the next step was to shut the engine down for precaution. We checked WX in tul and mkc and both WX reports were good. We shut engine down and started a descent to do a straight-in approach to mkc on runway 1. The approach and landing were normal.
Original NASA ASRS Text
Title: FLC OF AN MLG ACR ACFT DIVERTED TO LAND AFTER SHUTTING DOWN AN ENG AT HIGH ALT CRUISE DUE TO A CSD LOW OIL PRESSURE PROB. INFLT ENG SHUTDOWN.
Narrative: BTWN TUL AND MKC, THE CSD OIL PRESSURE LOW LIGHT CAME ON. WE VERIFIED AND DID THE CHKLIST WHICH SAID TO DISCONNECT CSD. AFTER TRYING TO DISCONNECT CSD, WITHOUT ANY LUCK, THE NEXT STEP WAS TO SHUT THE ENG DOWN FOR PRECAUTION. WE CHKED WX IN TUL AND MKC AND BOTH WX RPTS WERE GOOD. WE SHUT ENG DOWN AND STARTED A DSCNT TO DO A STRAIGHT-IN APCH TO MKC ON RWY 1. THE APCH AND LNDG WERE NORMAL.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.