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|
Attributes | |
ACN | 280050 |
Time | |
Date | 199408 |
Day | Thu |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : yip |
State Reference | MI |
Altitude | msl bound lower : 4000 msl bound upper : 4000 |
Environment | |
Flight Conditions | IMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : yip tower : yip |
Operator | common carrier : air taxi |
Make Model Name | Commercial Fixed Wing |
Operating Under FAR Part | Part 135 |
Flight Phase | cruise other descent : approach landing other |
Route In Use | arrival other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air taxi |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : cfi pilot : instrument |
Experience | flight time last 90 days : 200 flight time total : 4300 flight time type : 150 |
ASRS Report | 280050 |
Person 2 | |
Affiliation | company : air taxi |
Function | flight crew : captain oversight : pic |
Qualification | pilot : cfi pilot : atp |
Experience | flight time total : 4600 |
ASRS Report | 280049 |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | other controllera other flight crewa |
Resolutory Action | flight crew : declared emergency flight crew : overcame equipment problem flight crew : returned to intended course or assigned course other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
The aircraft was having intermittent radio problems and eventually all radios stayed 'hot.' the radios lost communication when switching over to detroit approach. At this point we squawked 7600 and proceeded as per last communication procedures. Regained radio reception during final approach segment, and received landing clearance. The WX was the contributing factor. Rain was leaking through the nose of the aircraft which caused the radios to get wet and short out. It was discovered when we lost reception and were informed of the 'hot microphone' situation once reception was restored. Before our departure, both radios appeared to be working normally. When trouble-shooting, we had no indication on one side that mikes were hot. When we were first experiencing difficulties, no one informed us that we were transmitting. If we were informed of this, that would have made trouble-shooting with the proper corrective action easier. Although the actions of the flight crew were not perfect, I believe we reacted as most crews would have.
Original NASA ASRS Text
Title: AN ATX SMT HAD A COM FAILURE IN THE WX.
Narrative: THE ACFT WAS HAVING INTERMITTENT RADIO PROBS AND EVENTUALLY ALL RADIOS STAYED 'HOT.' THE RADIOS LOST COM WHEN SWITCHING OVER TO DETROIT APCH. AT THIS POINT WE SQUAWKED 7600 AND PROCEEDED AS PER LAST COM PROCS. REGAINED RADIO RECEPTION DURING FINAL APCH SEGMENT, AND RECEIVED LNDG CLRNC. THE WX WAS THE CONTRIBUTING FACTOR. RAIN WAS LEAKING THROUGH THE NOSE OF THE ACFT WHICH CAUSED THE RADIOS TO GET WET AND SHORT OUT. IT WAS DISCOVERED WHEN WE LOST RECEPTION AND WERE INFORMED OF THE 'HOT MIKE' SIT ONCE RECEPTION WAS RESTORED. BEFORE OUR DEP, BOTH RADIOS APPEARED TO BE WORKING NORMALLY. WHEN TROUBLE-SHOOTING, WE HAD NO INDICATION ON ONE SIDE THAT MIKES WERE HOT. WHEN WE WERE FIRST EXPERIENCING DIFFICULTIES, NO ONE INFORMED US THAT WE WERE XMITTING. IF WE WERE INFORMED OF THIS, THAT WOULD HAVE MADE TROUBLE-SHOOTING WITH THE PROPER CORRECTIVE ACTION EASIER. ALTHOUGH THE ACTIONS OF THE FLC WERE NOT PERFECT, I BELIEVE WE REACTED AS MOST CREWS WOULD HAVE.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.