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|
Attributes | |
ACN | 291601 |
Time | |
Date | 199412 |
Day | Thu |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : ord |
State Reference | IL |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Aircraft 1 | |
Controlling Facilities | artcc : rktt |
Operator | common carrier : air carrier |
Make Model Name | A320 |
Operating Under FAR Part | Part 121 |
Navigation In Use | Other Other |
Flight Phase | climbout : takeoff other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | other personnel other |
Qualification | other other : other |
ASRS Report | 291601 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | flight crew : rejected takeoff other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
On dec/xx/94 aircraft, an A-320, arrived at ord for overnight maintenance. A maintenance call was assigned to change a parking brake dual shuttle valve. The valve installed on the aircraft was on loan from air carrier Y. I removed and replaced the valves as per A-320 maintenance manuals. The system was operational checked and gear checked with no problems found. My shift ended before the aircraft departed. On takeoff roll an o-ring failed on the installed valve. Yellow system hydraulic fluid drained from the aircraft and the takeoff was aborted. The aircraft returned to the gate, at which time dayshift mechanics replaced the failed o- ring. The system was tested, found normal and the aircraft continued on revenue service. Very little could be done to avoid the situation. The valve installed was installed in the condition as delivered. No o-rings were disturbed at ord that night. All maintenance manuals were followed. I feel this incident was out of the control of the person/persons involved. I feel there were no other actions available to stop this from happening.
Original NASA ASRS Text
Title: FLC OF AN MLG ABORTED TKOF DUE TO HYD FLUID LOSS.
Narrative: ON DEC/XX/94 ACFT, AN A-320, ARRIVED AT ORD FOR OVERNIGHT MAINT. A MAINT CALL WAS ASSIGNED TO CHANGE A PARKING BRAKE DUAL SHUTTLE VALVE. THE VALVE INSTALLED ON THE ACFT WAS ON LOAN FROM ACR Y. I REMOVED AND REPLACED THE VALVES AS PER A-320 MAINT MANUALS. THE SYS WAS OPERATIONAL CHKED AND GEAR CHKED WITH NO PROBS FOUND. MY SHIFT ENDED BEFORE THE ACFT DEPARTED. ON TKOF ROLL AN O-RING FAILED ON THE INSTALLED VALVE. YELLOW SYS HYD FLUID DRAINED FROM THE ACFT AND THE TKOF WAS ABORTED. THE ACFT RETURNED TO THE GATE, AT WHICH TIME DAYSHIFT MECHS REPLACED THE FAILED O- RING. THE SYS WAS TESTED, FOUND NORMAL AND THE ACFT CONTINUED ON REVENUE SVC. VERY LITTLE COULD BE DONE TO AVOID THE SIT. THE VALVE INSTALLED WAS INSTALLED IN THE CONDITION AS DELIVERED. NO O-RINGS WERE DISTURBED AT ORD THAT NIGHT. ALL MAINT MANUALS WERE FOLLOWED. I FEEL THIS INCIDENT WAS OUT OF THE CTL OF THE PERSON/PERSONS INVOLVED. I FEEL THERE WERE NO OTHER ACTIONS AVAILABLE TO STOP THIS FROM HAPPENING.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.