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|
Attributes | |
ACN | 294120 |
Time | |
Date | 199501 |
Day | Thu |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : mem |
State Reference | TN |
Altitude | msl bound lower : 2000 msl bound upper : 2000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : mem tower : cvg |
Operator | common carrier : air carrier |
Make Model Name | Commercial Fixed Wing |
Operating Under FAR Part | Part 121 |
Flight Phase | climbout : initial other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : instrument pilot : atp |
Experience | flight time last 90 days : 200 flight time total : 8000 flight time type : 5000 |
ASRS Report | 294120 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | Pilot Deviation |
Narrative:
I, the copilot, reported to work prior to required check-in at XG50 local and pulled up ewr WX. Since the WX was bad at ewr, I proceeded to the aircraft and performed my preflight at approximately XH05-XH10 local completing it in approximately 6-8 mins. All gear doors were up and the bypass lever was fully stowed. The maintenance personnel were in the process of beginning a daily inspection when I returned to the cockpit after my exterior preflight. I did this preflight early so I could check on our air traffic delay to ewr. We departed the gate at XI21 local, and during taxi and the takeoff roll all indications and lights were normal. Upon rotation and gear retraction, the gear would not retract and the door open light was now on. Company communication procedures were accomplished while staying VFR and in the local area. Maintenance was consulted prior to landing. An uneventful lng on runway 27 was accomplished. Doors were retracted by maintenance and the gear pinned prior to taxi clear of runway and back to the gate. The logbook, upon inspection after this, indicated the daily was done at XG30Z however, the aircraft did not land at mem from aus until XG58Z. The entry probably was an addition error and should have read XH30Z. At no time were individuals in danger. The maintenance bypass lever on the bottom of the aircraft was found extended. This lever was stowed at the time of my preflight but is utilized by maintenance to perform them daily inspections. It may not have been fully latched after their use and rotation forces pulled the lever to the extend position.
Original NASA ASRS Text
Title: FLC OF AN MLG RETURNED TO LAND AFTER THE LNDG GEAR FAILED TO RETRACT PROPERLY.
Narrative: I, THE COPLT, RPTED TO WORK PRIOR TO REQUIRED CHK-IN AT XG50 LCL AND PULLED UP EWR WX. SINCE THE WX WAS BAD AT EWR, I PROCEEDED TO THE ACFT AND PERFORMED MY PREFLT AT APPROX XH05-XH10 LCL COMPLETING IT IN APPROX 6-8 MINS. ALL GEAR DOORS WERE UP AND THE BYPASS LEVER WAS FULLY STOWED. THE MAINT PERSONNEL WERE IN THE PROCESS OF BEGINNING A DAILY INSPECTION WHEN I RETURNED TO THE COCKPIT AFTER MY EXTERIOR PREFLT. I DID THIS PREFLT EARLY SO I COULD CHK ON OUR AIR TFC DELAY TO EWR. WE DEPARTED THE GATE AT XI21 LCL, AND DURING TAXI AND THE TKOF ROLL ALL INDICATIONS AND LIGHTS WERE NORMAL. UPON ROTATION AND GEAR RETRACTION, THE GEAR WOULD NOT RETRACT AND THE DOOR OPEN LIGHT WAS NOW ON. COMPANY COM PROCS WERE ACCOMPLISHED WHILE STAYING VFR AND IN THE LCL AREA. MAINT WAS CONSULTED PRIOR TO LNDG. AN UNEVENTFUL LNG ON RWY 27 WAS ACCOMPLISHED. DOORS WERE RETRACTED BY MAINT AND THE GEAR PINNED PRIOR TO TAXI CLR OF RWY AND BACK TO THE GATE. THE LOGBOOK, UPON INSPECTION AFTER THIS, INDICATED THE DAILY WAS DONE AT XG30Z HOWEVER, THE ACFT DID NOT LAND AT MEM FROM AUS UNTIL XG58Z. THE ENTRY PROBABLY WAS AN ADDITION ERROR AND SHOULD HAVE READ XH30Z. AT NO TIME WERE INDIVIDUALS IN DANGER. THE MAINT BYPASS LEVER ON THE BOTTOM OF THE ACFT WAS FOUND EXTENDED. THIS LEVER WAS STOWED AT THE TIME OF MY PREFLT BUT IS UTILIZED BY MAINT TO PERFORM THEM DAILY INSPECTIONS. IT MAY NOT HAVE BEEN FULLY LATCHED AFTER THEIR USE AND ROTATION FORCES PULLED THE LEVER TO THE EXTEND POS.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.