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|
Attributes | |
ACN | 302348 |
Time | |
Date | 199504 |
Day | Thu |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | atc facility : vuz |
State Reference | AZ |
Altitude | msl bound lower : 8500 msl bound upper : 8500 |
Environment | |
Flight Conditions | VMC |
Light | Dusk |
Aircraft 1 | |
Controlling Facilities | artcc : ztl |
Operator | common carrier : air carrier |
Make Model Name | Commercial Fixed Wing |
Operating Under FAR Part | Part 121 |
Navigation In Use | Other Other |
Flight Phase | climbout : intermediate altitude |
Route In Use | enroute airway : ztl |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp pilot : cfi |
Experience | flight time last 90 days : 300 flight time total : 13000 flight time type : 300 |
ASRS Report | 302348 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : cfi pilot : commercial pilot : instrument pilot : flight engineer |
Experience | flight time last 90 days : 210 flight time total : 7500 flight time type : 210 |
ASRS Report | 301651 |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | flight crew : declared emergency none taken : unable none taken : anomaly accepted |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
During climb out at 8500 ft, left engine failed indicated by a loud thump and yaw to left, along with rapidly rising temperature indication. Engine was shutdown in accordance with appropriate checklists, emergency was declared with controling facility, and request for return to nearest suitable airport made - bhm. Appropriate checklists were completed, and single engine landing was uneventfully made. Crew coordination was superb! Left engine was now windmilling and causing a very bad vibration so I adjusted the pitch of the propeller using the propeller auxiliary pump and the vibration immediately stopped. The vibration gradually came back as the propeller adjusted itself to its former feathered position. There is no procedure for this, but it did work.
Original NASA ASRS Text
Title: ENG FAILURE DURING CLBOUT.
Narrative: DURING CLBOUT AT 8500 FT, L ENG FAILED INDICATED BY A LOUD THUMP AND YAW TO L, ALONG WITH RAPIDLY RISING TEMP INDICATION. ENG WAS SHUTDOWN IN ACCORDANCE WITH APPROPRIATE CHKLISTS, EMER WAS DECLARED WITH CTLING FACILITY, AND REQUEST FOR RETURN TO NEAREST SUITABLE ARPT MADE - BHM. APPROPRIATE CHKLISTS WERE COMPLETED, AND SINGLE ENG LNDG WAS UNEVENTFULLY MADE. CREW COORD WAS SUPERB! L ENG WAS NOW WINDMILLING AND CAUSING A VERY BAD VIBRATION SO I ADJUSTED THE PITCH OF THE PROP USING THE PROP AUX PUMP AND THE VIBRATION IMMEDIATELY STOPPED. THE VIBRATION GRADUALLY CAME BACK AS THE PROP ADJUSTED ITSELF TO ITS FORMER FEATHERED POS. THERE IS NO PROC FOR THIS, BUT IT DID WORK.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.