Narrative:

Rudder position indicated approximately 3 1/2 - 4 degrees left. Required 4 degree right wing down aileron trim to maintain course. No warning lights at any time nor any other abnormal indications. Normal hydraulics, etc. Problem found by mechanic in slc to be binding of captain rudder pedal mechanism. Flight proceeded cvg to slc without incident. Supplemental information from acn 330586: problem was discovered to be in the captain's rudder pedal adjustment mechanism. Possibly the teleflex cable becoming worn and frayed.

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Original NASA ASRS Text

Title: RUDDER POS INDICATOR DEFLECTED DUE TO BINDING RUDDER PEDAL. FLT CONTINUED USING WING DOWN AILERON TRIM TO COMPENSATE. MECH FOUND THE PROB AND REPAIRED.

Narrative: RUDDER POS INDICATED APPROX 3 1/2 - 4 DEGS L. REQUIRED 4 DEG R WING DOWN AILERON TRIM TO MAINTAIN COURSE. NO WARNING LIGHTS AT ANY TIME NOR ANY OTHER ABNORMAL INDICATIONS. NORMAL HYDS, ETC. PROB FOUND BY MECH IN SLC TO BE BINDING OF CAPT RUDDER PEDAL MECHANISM. FLT PROCEEDED CVG TO SLC WITHOUT INCIDENT. SUPPLEMENTAL INFO FROM ACN 330586: PROB WAS DISCOVERED TO BE IN THE CAPT'S RUDDER PEDAL ADJUSTMENT MECHANISM. POSSIBLY THE TELEFLEX CABLE BECOMING WORN AND FRAYED.

Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.