37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 362519 |
Time | |
Date | 199703 |
Day | Sun |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | atc facility : dfw airport : dtw |
State Reference | TX |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tower : mkc |
Operator | common carrier : air carrier |
Make Model Name | MD-88 |
Operating Under FAR Part | Part 121 |
Navigation In Use | Other Other |
Flight Phase | landing other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : flight engineer pilot : atp |
Experience | flight time last 90 days : 150 flight time total : 6600 flight time type : 3000 |
ASRS Report | 362519 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : critical inflight encounter : weather |
Independent Detector | aircraft equipment other aircraft equipment : unspecified |
Resolutory Action | none taken : anomaly accepted |
Consequence | other |
Supplementary | |
Primary Problem | Flight Crew Human Performance |
Air Traffic Incident | Pilot Deviation |
Narrative:
After gear extension, the gear door unlocked light failed to go out. This was recognized at 1200 ft AGL while running the before landing checklist. There wasn't time to run the abnormal checklist, obviously, without go around and due to thunderstorms all over the area (including hail we had encountered on 12 mi final, which we couldn't see and didn't show up on the radar), the captain elected to land. We also felt there was a good chance the door would float as it does when alternate gear extension is used (if malfunction was in light switch or door lock). The landing was absolutely normal from the cockpit. No unusual sounds, feelings, etc. No comments from the flight attendants or passenger (except for 'nice landing'). It turned out the door was open on landing. It impacted the runway bending the door and grinding part of it away. The malfunction was a broken sequencing linkage that caused the door to stay open.
Original NASA ASRS Text
Title: MD88 FLC IGNORED A GEAR DOOR UNLOCKED WARNING LIGHT THINKING IT WAS A FALSE ALARM OR THAT THE GEAR DOOR WOULD FLOAT AND JUST LIGHTLY TOUCH THE RWY AT THE END OF THE LNDG ROLL. INSTEAD, THE DOOR WAS DAMAGED UPON LNDG. THEY WERE CONCERNED ABOUT TSTMS IN THE AREA AND DECIDED NOT TO GO AROUND AND FOLLOW THE HANDBOOK PROC.
Narrative: AFTER GEAR EXTENSION, THE GEAR DOOR UNLOCKED LIGHT FAILED TO GO OUT. THIS WAS RECOGNIZED AT 1200 FT AGL WHILE RUNNING THE BEFORE LNDG CHKLIST. THERE WASN'T TIME TO RUN THE ABNORMAL CHKLIST, OBVIOUSLY, WITHOUT GAR AND DUE TO TSTMS ALL OVER THE AREA (INCLUDING HAIL WE HAD ENCOUNTERED ON 12 MI FINAL, WHICH WE COULDN'T SEE AND DIDN'T SHOW UP ON THE RADAR), THE CAPT ELECTED TO LAND. WE ALSO FELT THERE WAS A GOOD CHANCE THE DOOR WOULD FLOAT AS IT DOES WHEN ALTERNATE GEAR EXTENSION IS USED (IF MALFUNCTION WAS IN LIGHT SWITCH OR DOOR LOCK). THE LNDG WAS ABSOLUTELY NORMAL FROM THE COCKPIT. NO UNUSUAL SOUNDS, FEELINGS, ETC. NO COMMENTS FROM THE FLT ATTENDANTS OR PAX (EXCEPT FOR 'NICE LNDG'). IT TURNED OUT THE DOOR WAS OPEN ON LNDG. IT IMPACTED THE RWY BENDING THE DOOR AND GRINDING PART OF IT AWAY. THE MALFUNCTION WAS A BROKEN SEQUENCING LINKAGE THAT CAUSED THE DOOR TO STAY OPEN.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.