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|
Attributes | |
ACN | 362830 |
Time | |
Date | 199703 |
Day | Thu |
Local Time Of Day | 0001 To 0600 |
Place | |
Locale Reference | atc facility : tvc |
State Reference | MI |
Altitude | agl bound lower : 0 agl bound upper : 0 msl bound lower : 31000 msl bound upper : 35000 |
Environment | |
Flight Conditions | VMC |
Light | Night |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | B747-C/F |
Operating Under FAR Part | Part 121 |
Flight Phase | cruise other |
Route In Use | enroute airway : chi |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain |
Qualification | pilot : instrument pilot : commercial pilot : atp |
Experience | flight time last 90 days : 100 flight time total : 13000 flight time type : 1200 |
ASRS Report | 362830 |
Person 2 | |
Affiliation | company : air carrier |
Function | observation : company check pilot oversight : pic |
Qualification | pilot : instrument pilot : commercial pilot : atp |
Events | |
Anomaly | aircraft equipment problem : critical non adherence : far non adherence : published procedure other anomaly other |
Independent Detector | other flight crewa other other : unspecified cockpit |
Resolutory Action | other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | Pilot Deviation |
Narrative:
Upon level off at FL310, flight engineer discovered #3 main tank fuel quantity gauge stuck at 61000 pounds. Since #3 and #2 are identical, he did some troubleshooting and swapped quantity gauges. Upon discovering that the problem was neither gauge, he swapped them back to original position. #3 gauge then stuck at 46000 pounds. About 4 1/2 hours into planned 6 hour flight, #3 forward boost pump low pressure light came on. Aircraft attitude was approximately 2 1/2 degrees nose up. In order to check fuel quantity in #3 tank, #3 tank jettison/transfer pumps were turned on. Low pressure lights came on for those pumps also, indicating fuel quantity in that tank to be below standpipe level. Quantity gauging system for #3 tank had been worked on at home station on feb/xx/96, changing sensing harness and other components. There were no logbook entries about this system since that date. Destination was jfk, which was reporting instrument WX conditions. Upon discussion among the crew, and phone patch with company dispatch and maintenance control, flight diverted to ord. We landed with 31600 pounds, 2200 pounds in #3 main tank.
Original NASA ASRS Text
Title: A B747 IN CARGO CONFIGN DIVERTED DUE TO INSUFFICIENT FUEL IN #3 MAIN TANK.
Narrative: UPON LEVEL OFF AT FL310, FE DISCOVERED #3 MAIN TANK FUEL QUANTITY GAUGE STUCK AT 61000 LBS. SINCE #3 AND #2 ARE IDENTICAL, HE DID SOME TROUBLESHOOTING AND SWAPPED QUANTITY GAUGES. UPON DISCOVERING THAT THE PROB WAS NEITHER GAUGE, HE SWAPPED THEM BACK TO ORIGINAL POS. #3 GAUGE THEN STUCK AT 46000 LBS. ABOUT 4 1/2 HRS INTO PLANNED 6 HR FLT, #3 FORWARD BOOST PUMP LOW PRESSURE LIGHT CAME ON. ACFT ATTITUDE WAS APPROX 2 1/2 DEGS NOSE UP. IN ORDER TO CHK FUEL QUANTITY IN #3 TANK, #3 TANK JETTISON/TRANSFER PUMPS WERE TURNED ON. LOW PRESSURE LIGHTS CAME ON FOR THOSE PUMPS ALSO, INDICATING FUEL QUANTITY IN THAT TANK TO BE BELOW STANDPIPE LEVEL. QUANTITY GAUGING SYS FOR #3 TANK HAD BEEN WORKED ON AT HOME STATION ON FEB/XX/96, CHANGING SENSING HARNESS AND OTHER COMPONENTS. THERE WERE NO LOGBOOK ENTRIES ABOUT THIS SYS SINCE THAT DATE. DEST WAS JFK, WHICH WAS RPTING INST WX CONDITIONS. UPON DISCUSSION AMONG THE CREW, AND PHONE PATCH WITH COMPANY DISPATCH AND MAINT CTL, FLT DIVERTED TO ORD. WE LANDED WITH 31600 LBS, 2200 LBS IN #3 MAIN TANK.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.