Narrative:

Upon level off at FL310, flight engineer discovered #3 main tank fuel quantity gauge stuck at 61000 pounds. Since #3 and #2 are identical, he did some troubleshooting and swapped quantity gauges. Upon discovering that the problem was neither gauge, he swapped them back to original position. #3 gauge then stuck at 46000 pounds. About 4 1/2 hours into planned 6 hour flight, #3 forward boost pump low pressure light came on. Aircraft attitude was approximately 2 1/2 degrees nose up. In order to check fuel quantity in #3 tank, #3 tank jettison/transfer pumps were turned on. Low pressure lights came on for those pumps also, indicating fuel quantity in that tank to be below standpipe level. Quantity gauging system for #3 tank had been worked on at home station on feb/xx/96, changing sensing harness and other components. There were no logbook entries about this system since that date. Destination was jfk, which was reporting instrument WX conditions. Upon discussion among the crew, and phone patch with company dispatch and maintenance control, flight diverted to ord. We landed with 31600 pounds, 2200 pounds in #3 main tank.

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Original NASA ASRS Text

Title: A B747 IN CARGO CONFIGN DIVERTED DUE TO INSUFFICIENT FUEL IN #3 MAIN TANK.

Narrative: UPON LEVEL OFF AT FL310, FE DISCOVERED #3 MAIN TANK FUEL QUANTITY GAUGE STUCK AT 61000 LBS. SINCE #3 AND #2 ARE IDENTICAL, HE DID SOME TROUBLESHOOTING AND SWAPPED QUANTITY GAUGES. UPON DISCOVERING THAT THE PROB WAS NEITHER GAUGE, HE SWAPPED THEM BACK TO ORIGINAL POS. #3 GAUGE THEN STUCK AT 46000 LBS. ABOUT 4 1/2 HRS INTO PLANNED 6 HR FLT, #3 FORWARD BOOST PUMP LOW PRESSURE LIGHT CAME ON. ACFT ATTITUDE WAS APPROX 2 1/2 DEGS NOSE UP. IN ORDER TO CHK FUEL QUANTITY IN #3 TANK, #3 TANK JETTISON/TRANSFER PUMPS WERE TURNED ON. LOW PRESSURE LIGHTS CAME ON FOR THOSE PUMPS ALSO, INDICATING FUEL QUANTITY IN THAT TANK TO BE BELOW STANDPIPE LEVEL. QUANTITY GAUGING SYS FOR #3 TANK HAD BEEN WORKED ON AT HOME STATION ON FEB/XX/96, CHANGING SENSING HARNESS AND OTHER COMPONENTS. THERE WERE NO LOGBOOK ENTRIES ABOUT THIS SYS SINCE THAT DATE. DEST WAS JFK, WHICH WAS RPTING INST WX CONDITIONS. UPON DISCUSSION AMONG THE CREW, AND PHONE PATCH WITH COMPANY DISPATCH AND MAINT CTL, FLT DIVERTED TO ORD. WE LANDED WITH 31600 LBS, 2200 LBS IN #3 MAIN TANK.

Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.