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|
Attributes | |
ACN | 399054 |
Time | |
Date | 199804 |
Day | Fri |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : slc |
State Reference | UT |
Altitude | agl bound lower : 0 agl bound upper : 500 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tower : slc tower : bdl |
Operator | common carrier : air carrier |
Make Model Name | B727 Undifferentiated or Other Model |
Operating Under FAR Part | Part 121 |
Flight Phase | climbout : takeoff climbout : initial other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp pilot : flight engineer |
Experience | flight time last 90 days : 180 flight time total : 13000 flight time type : 4800 |
ASRS Report | 399054 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : instrument pilot : commercial |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | flight crew : regained aircraft control none taken : detected after the fact other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
We boarded the flight to find a write-up by the inbound crew for a compressor stall on #3 engine during takeoff at the previous airport. Our mechanic had signed it off after an inspection and informed us that he'd found no damage or reason for the stall. We were scheduled for a pair of flts, out to a city with no company maintenance, and back. With this in mind, along with the fact that no apparent reason for the stall had been discovered, we decided to return for landing if it happened to us. It, of course, did. After a normal taxi and takeoff roll, #3 engine 'popped' twice during rotation before liftoff. Power was reduced and the stall cleared. Engine shutdown was not necessary and we turned downwind for landing as planned. Fuel dump was not necessary and all checklists were complied with. The copilot was PF during the takeoff, and he continued to fly for the duration. It was a very busy flight segment made manageable because we had already discussed.
Original NASA ASRS Text
Title: A B727 DEPARTING SLC HAS AN ENG COMPRESSOR STALL DURING TKOF ROTATION. FLC REDUCES PWR AND RETURN LAND.
Narrative: WE BOARDED THE FLT TO FIND A WRITE-UP BY THE INBOUND CREW FOR A COMPRESSOR STALL ON #3 ENG DURING TKOF AT THE PREVIOUS ARPT. OUR MECH HAD SIGNED IT OFF AFTER AN INSPECTION AND INFORMED US THAT HE'D FOUND NO DAMAGE OR REASON FOR THE STALL. WE WERE SCHEDULED FOR A PAIR OF FLTS, OUT TO A CITY WITH NO COMPANY MAINT, AND BACK. WITH THIS IN MIND, ALONG WITH THE FACT THAT NO APPARENT REASON FOR THE STALL HAD BEEN DISCOVERED, WE DECIDED TO RETURN FOR LNDG IF IT HAPPENED TO US. IT, OF COURSE, DID. AFTER A NORMAL TAXI AND TKOF ROLL, #3 ENG 'POPPED' TWICE DURING ROTATION BEFORE LIFTOFF. PWR WAS REDUCED AND THE STALL CLRED. ENG SHUTDOWN WAS NOT NECESSARY AND WE TURNED DOWNWIND FOR LNDG AS PLANNED. FUEL DUMP WAS NOT NECESSARY AND ALL CHKLISTS WERE COMPLIED WITH. THE COPLT WAS PF DURING THE TKOF, AND HE CONTINUED TO FLY FOR THE DURATION. IT WAS A VERY BUSY FLT SEGMENT MADE MANAGEABLE BECAUSE WE HAD ALREADY DISCUSSED.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.