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|
Attributes | |
ACN | 456018 |
Time | |
Date | 199911 |
Day | Tue |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : slc.airport |
State Reference | UT |
Altitude | agl single value : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | B727 Undifferentiated or Other Model |
Flight Phase | climbout : takeoff |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : second officer |
Qualification | pilot : atp pilot : flight engineer |
Experience | flight time last 90 days : 210 flight time total : 5500 flight time type : 1500 |
ASRS Report | 456018 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | other flight crewa other flight crewb |
Resolutory Action | flight crew : landed in emergency condition flight crew : declared emergency other |
Consequence | other other other |
Supplementary | |
Problem Areas | Aircraft |
Primary Problem | Aircraft |
Narrative:
During takeoff roll at approximately 120 KTS, the #1 engine EPR dropped. It was accompanied by popping sounds heard by aft flight attendants and low bleed air duct pressure from the engine. At cruise power settings, engine indications appeared normal. After discussions with company maintenance, it was determined a return to slc was the best course of action. We dumped fuel to get down to normal landing weight. After uneventful landing we turned the aircraft over to maintenance. Supplemental information from acn 455752: fuel was dumped to maximum landing weight, emergency was declared, and an uneventful landing made.
Original NASA ASRS Text
Title: A B727 FLC RETURNS AND LANDS WHEN THE #1 ENG IS SUSPECTED OF A MALFUNCTION AT SLC, UT.
Narrative: DURING TKOF ROLL AT APPROX 120 KTS, THE #1 ENG EPR DROPPED. IT WAS ACCOMPANIED BY POPPING SOUNDS HEARD BY AFT FLT ATTENDANTS AND LOW BLEED AIR DUCT PRESSURE FROM THE ENG. AT CRUISE PWR SETTINGS, ENG INDICATIONS APPEARED NORMAL. AFTER DISCUSSIONS WITH COMPANY MAINT, IT WAS DETERMINED A RETURN TO SLC WAS THE BEST COURSE OF ACTION. WE DUMPED FUEL TO GET DOWN TO NORMAL LNDG WT. AFTER UNEVENTFUL LNDG WE TURNED THE ACFT OVER TO MAINT. SUPPLEMENTAL INFO FROM ACN 455752: FUEL WAS DUMPED TO MAX LNDG WT, EMER WAS DECLARED, AND AN UNEVENTFUL LNDG MADE.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.