37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 462273 |
Time | |
Date | 200002 |
Day | Fri |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | atc facility : zau.artcc |
State Reference | IL |
Environment | |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : zau.artcc |
Operator | common carrier : air carrier |
Make Model Name | B767-300 and 300 ER |
Operating Under FAR Part | Part 121 |
Flight Phase | climbout : initial climbout : takeoff cruise : holding landing other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight attendant : on duty |
Qualification | flight attendant : currently qualified flight attendant aircraft qualified on : 7 |
Experience | flight attendant time airline total : 27 flight attendant time total : 27 flight attendant time type : 90 |
ASRS Report | 462273 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : landed as precaution flight crew : landed in emergency condition flight crew : diverted to alternate |
Consequence | other |
Supplementary | |
Problem Areas | Aircraft |
Primary Problem | Aircraft |
Narrative:
After takeoff, we were informed that there was a flap problem and that we were going back to chicago -- our time in the air was about 45 mins. We flew for a little while and the crew tried to fix the problem, but couldn't. The cockpit kept passenger well informed. Cabin crew was very calm. Considering our fuel weight, the landing was excellent.
Original NASA ASRS Text
Title: CABIN ATTENDANT RPT, B767-300, ORD-LHR. AFTER TKOF, FLAP PROB. FLC TRIED TO FIX IN AIR, CIRCLE 45 MINS. RETURN TO ORD. OVERWT LNDG.
Narrative: AFTER TKOF, WE WERE INFORMED THAT THERE WAS A FLAP PROB AND THAT WE WERE GOING BACK TO CHICAGO -- OUR TIME IN THE AIR WAS ABOUT 45 MINS. WE FLEW FOR A LITTLE WHILE AND THE CREW TRIED TO FIX THE PROB, BUT COULDN'T. THE COCKPIT KEPT PAX WELL INFORMED. CABIN CREW WAS VERY CALM. CONSIDERING OUR FUEL WT, THE LNDG WAS EXCELLENT.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.