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Attributes | |
ACN | 502530 |
Time | |
Date | 200102 |
Day | Fri |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : dfw.airport |
State Reference | TX |
Altitude | agl single value : 0 |
Environment | |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | Fokker 100 |
Operating Under FAR Part | Part 121 |
Flight Phase | ground : parked ground other : engine start |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
ASRS Report | 502530 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : instrument pilot : multi engine |
Events | |
Anomaly | aircraft equipment problem : less severe other anomaly other |
Independent Detector | other flight crewa other flight crewb |
Resolutory Action | other |
Consequence | other other |
Supplementary | |
Problem Areas | Company Aircraft |
Primary Problem | Company |
Narrative:
APU lost pressure output. Arrived at the aircraft, checked the logbook -- clean. Completed checklist, prepared for a start to pwrback. Attempted to start #1. Due to low pressure, aborted start. Copilot asked if I wanted to call maintenance. I said 'no, ask for a tart cart.' I considered that reasonable due to the warm gusty conditions. Due to the position of the aircraft, there was also a tailwind. Hooked up the start cart, started engines and left. Wrong decision. Arrived at oma, started the APU, then noticed the pressure once again lower than normal. Turned off the packs. Pressure appeared to be normal around 44 psi. I elected to call maintenance as I was unsure as to the integrity of the system. The APU was placarded by contract maintenance. We incurred a 2 1/2 hour delay due to my wrong decision at the start. Had we called maintenance in dfw, sure we would have been delayed more, but not as long as our delay in oma. I guess part of my reasoning included that we were already 1 hour behind due to WX, due to a different aircraft with similar problems. I guess, in trying so hard not to make a wrong decision, I made a wrong decision.
Original NASA ASRS Text
Title: F100 CREW HAD LOW APU PNEUMATIC PRESSURE DURING ENG START.
Narrative: APU LOST PRESSURE OUTPUT. ARRIVED AT THE ACFT, CHKED THE LOGBOOK -- CLEAN. COMPLETED CHKLIST, PREPARED FOR A START TO PWRBACK. ATTEMPTED TO START #1. DUE TO LOW PRESSURE, ABORTED START. COPLT ASKED IF I WANTED TO CALL MAINT. I SAID 'NO, ASK FOR A TART CART.' I CONSIDERED THAT REASONABLE DUE TO THE WARM GUSTY CONDITIONS. DUE TO THE POSITION OF THE ACFT, THERE WAS ALSO A TAILWIND. HOOKED UP THE START CART, STARTED ENGS AND LEFT. WRONG DECISION. ARRIVED AT OMA, STARTED THE APU, THEN NOTICED THE PRESSURE ONCE AGAIN LOWER THAN NORMAL. TURNED OFF THE PACKS. PRESSURE APPEARED TO BE NORMAL AROUND 44 PSI. I ELECTED TO CALL MAINT AS I WAS UNSURE AS TO THE INTEGRITY OF THE SYS. THE APU WAS PLACARDED BY CONTRACT MAINT. WE INCURRED A 2 1/2 HR DELAY DUE TO MY WRONG DECISION AT THE START. HAD WE CALLED MAINT IN DFW, SURE WE WOULD HAVE BEEN DELAYED MORE, BUT NOT AS LONG AS OUR DELAY IN OMA. I GUESS PART OF MY REASONING INCLUDED THAT WE WERE ALREADY 1 HR BEHIND DUE TO WX, DUE TO A DIFFERENT ACFT WITH SIMILAR PROBS. I GUESS, IN TRYING SO HARD NOT TO MAKE A WRONG DECISION, I MADE A WRONG DECISION.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.