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|
Attributes | |
ACN | 638188 |
Time | |
Date | 200411 |
Day | Wed |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : ord.airport |
State Reference | IL |
Altitude | msl single value : 8000 |
Environment | |
Flight Conditions | IMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : c90.tracon |
Operator | common carrier : air carrier |
Make Model Name | EMB ERJ 145 ER&LR |
Operating Under FAR Part | Part 121 |
Flight Phase | climbout : intermediate altitude landing : roll |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
ASRS Report | 638188 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Events | |
Anomaly | aircraft equipment problem : critical non adherence : company policies non adherence : far non adherence : published procedure other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : eicas bleed air warning other flight crewa |
Resolutory Action | controller : issued new clearance other |
Consequence | other other |
Factors | |
Maintenance | performance deficiency : logbook entry performance deficiency : non compliance with legal requirements performance deficiency : inspection |
Supplementary | |
Problem Areas | Aircraft Flight Crew Human Performance |
Primary Problem | Flight Crew Human Performance |
Narrative:
Departed for XXX following normal preflight and taxi. First officer's leg. Climbing through 8000 ft in IMC, we received a bleed 2 leak. Decided to return to ord after running appropriate checklists. I took my landing weight off of the performance page of the FMS. It was wrong, but I did not catch it. First officer flew until we were on the approach. I did the landing. I estimated about 150 FPM sink at touchdown. Debriefed maintenance at gate while crew and passenger moved to new airplane. Dispatch asked if I landed overweight. I said no. I believed that. During subsequent flight, I began to doubt my belief. Upon return to ord, I went to maintenance and checked on the landing fuel. Doing the math from memory, I am sure we were overweight -- 1500-2000 pounds. I then wrote the jet up for an overweight landing. Aircraft had not flown again.
Original NASA ASRS Text
Title: E145 FLT CREW INADVERTENTLY LAND OVERWT FOLLOWING DISCOVERY OF A BLEED AIR LEAK SOON AFTER DEP FROM ORD.
Narrative: DEPARTED FOR XXX FOLLOWING NORMAL PREFLT AND TAXI. FO'S LEG. CLBING THROUGH 8000 FT IN IMC, WE RECEIVED A BLEED 2 LEAK. DECIDED TO RETURN TO ORD AFTER RUNNING APPROPRIATE CHKLISTS. I TOOK MY LNDG WT OFF OF THE PERFORMANCE PAGE OF THE FMS. IT WAS WRONG, BUT I DID NOT CATCH IT. FO FLEW UNTIL WE WERE ON THE APCH. I DID THE LNDG. I ESTIMATED ABOUT 150 FPM SINK AT TOUCHDOWN. DEBRIEFED MAINT AT GATE WHILE CREW AND PAX MOVED TO NEW AIRPLANE. DISPATCH ASKED IF I LANDED OVERWT. I SAID NO. I BELIEVED THAT. DURING SUBSEQUENT FLT, I BEGAN TO DOUBT MY BELIEF. UPON RETURN TO ORD, I WENT TO MAINT AND CHKED ON THE LNDG FUEL. DOING THE MATH FROM MEMORY, I AM SURE WE WERE OVERWT -- 1500-2000 LBS. I THEN WROTE THE JET UP FOR AN OVERWT LNDG. ACFT HAD NOT FLOWN AGAIN.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.