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|
Attributes | |
ACN | 243759 |
Time | |
Date | 199306 |
Day | Sun |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : i39 |
State Reference | KY |
Altitude | msl bound lower : 9000 msl bound upper : 9000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : lex |
Operator | general aviation : personal |
Make Model Name | Small Aircraft, High Wing, 1 Eng, Fixed Gear |
Flight Phase | cruise other |
Route In Use | enroute : on vectors |
Flight Plan | IFR |
Person 1 | |
Affiliation | Other |
Function | flight crew : single pilot |
Qualification | pilot : instrument pilot : private |
Experience | flight time last 90 days : 33 flight time total : 340 flight time type : 240 |
ASRS Report | 243759 |
Person 2 | |
Affiliation | government : faa |
Function | controller : approach |
Qualification | controller : radar |
Events | |
Anomaly | aircraft equipment problem : critical other spatial deviation |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : declared emergency other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
Small aircraft was refueled in OI8. After preflight contacted lex approach to open IFR flight plan. Cleared to 9000 ft direct loz. Uneventful climb to 9000 ft. After approximately 45-60 min flight, light RPM changes then engine quit. Established best glide and notified lex approach who vectored me to I39. Mixture, carburetor heat, and throttle changes did not correct problem. Switched fuel selector to left with no result. After switching to right, power came back but with RPM variations. Landed at I39 ok. Mechanic checked out fuel system and found the right fuel vent blocked. Fuel selector valve was ok.
Original NASA ASRS Text
Title: SMA HAS ENG QUIT. SWITCHING FUEL TANKS ENABLES RESTART BUT RPM VARIABLE.
Narrative: SMA WAS REFUELED IN OI8. AFTER PREFLT CONTACTED LEX APCH TO OPEN IFR FLT PLAN. CLRED TO 9000 FT DIRECT LOZ. UNEVENTFUL CLB TO 9000 FT. AFTER APPROX 45-60 MIN FLT, LIGHT RPM CHANGES THEN ENG QUIT. ESTABLISHED BEST GLIDE AND NOTIFIED LEX APCH WHO VECTORED ME TO I39. MIXTURE, CARB HEAT, AND THROTTLE CHANGES DID NOT CORRECT PROB. SWITCHED FUEL SELECTOR TO L WITH NO RESULT. AFTER SWITCHING TO R, PWR CAME BACK BUT WITH RPM VARIATIONS. LANDED AT I39 OK. MECH CHKED OUT FUEL SYS AND FOUND THE R FUEL VENT BLOCKED. FUEL SELECTOR VALVE WAS OK.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.