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|
Attributes | |
ACN | 437535 |
Time | |
Date | 199905 |
Day | Mon |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | navaid : che.vortac |
State Reference | FO |
Altitude | msl single value : 31000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : rjtg.artcc |
Operator | common carrier : air carrier |
Make Model Name | B727-200 |
Operating Under FAR Part | Part 121 |
Navigation In Use | other |
Flight Phase | climbout : vacating altitude |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 250 flight time total : 16000 flight time type : 14000 |
ASRS Report | 437535 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : multi engine pilot : instrument pilot : commercial pilot : atp |
Experience | flight time last 90 days : 250 flight time total : 13000 flight time type : 3000 |
ASRS Report | 437959 |
Events | |
Anomaly | aircraft equipment problem : critical maintenance problem : improper maintenance non adherence : far non adherence : published procedure non adherence : company policies |
Independent Detector | other flight crewa |
Consequence | other |
Supplementary | |
Problem Areas | Maintenance Human Performance Aircraft |
Primary Problem | Maintenance Human Performance |
Narrative:
During climb the so noticed the oil qty in the #2 engine decreasing. Decision was made to return to cts. Appropriate checklists for oil qty loss and engine shutdown were accomplished. 17000 pounds of fuel dumped. Engine was shut down when oil qty reached .75 gals. Engine windmilled for 6 mins. Emergency was declared. Uneventful landing. Maintenance found a threaded plug for a service port on the engine driven gear box to be stripped causing the bolt to be loose. The corrective action would be for maintenance to avoid 'xthreading' or stripping bolts when installed, or correctly replacing or repairing the stripped bolt or socket.
Original NASA ASRS Text
Title: B727 CREW SHUT DOWN #2 ENG AFTER OIL LOSS.
Narrative: DURING CLB THE SO NOTICED THE OIL QTY IN THE #2 ENG DECREASING. DECISION WAS MADE TO RETURN TO CTS. APPROPRIATE CHKLISTS FOR OIL QTY LOSS AND ENG SHUTDOWN WERE ACCOMPLISHED. 17000 LBS OF FUEL DUMPED. ENG WAS SHUT DOWN WHEN OIL QTY REACHED .75 GALS. ENG WINDMILLED FOR 6 MINS. EMER WAS DECLARED. UNEVENTFUL LNDG. MAINT FOUND A THREADED PLUG FOR A SVC PORT ON THE ENG DRIVEN GEAR BOX TO BE STRIPPED CAUSING THE BOLT TO BE LOOSE. THE CORRECTIVE ACTION WOULD BE FOR MAINT TO AVOID 'XTHREADING' OR STRIPPING BOLTS WHEN INSTALLED, OR CORRECTLY REPLACING OR REPAIRING THE STRIPPED BOLT OR SOCKET.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.