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|
Attributes | |
ACN | 149395 |
Time | |
Date | 199006 |
Day | Wed |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : hou airport : aus |
State Reference | TX |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | Light Transport, Low Wing, 2 Turboprop Eng |
Flight Phase | climbout : takeoff |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
ASRS Report | 149395 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : second officer |
Qualification | pilot : commercial pilot : instrument |
Events | |
Anomaly | aircraft equipment problem : less severe non adherence : far |
Independent Detector | other flight crewa |
Resolutory Action | aircraft : equipment problem dissipated flight crew : overcame equipment problem |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
Upon arrival into the houston area we started our approach. When we extended the gear there were no indications of the 3 gear lights. We noticed that the gear indicator light circuit breaker was popped out. The copilot reset the circuit breaker and the 3 gear lights were illuminated. We flew by the tower to ensure the gear was down and they indicated that it was down. As a precautionary measure I told the tower to have the firetrucks standing by. We circled the airport and landed with no incident. On the ground, I called maintenance and was on the phone for approximately 5 mins. I waited until approximately 5 mins after departure time for a return phone call. I departed the aircraft to austin and neglected to communication with maintenance. Considering the passenger comfort and company schedule, we flew the aircraft to austin. Since the aircraft seemed to be airworthy being the only thing wrong was a circuit breaker that had popped out and was reset. The aircraft arrived in austin and there was nothing found wrong with it. Maintenance released the aircraft as airworthy.
Original NASA ASRS Text
Title: COMMUTER LTT FLT CREW FAILED TO MAKE A LOG BOOK ENTRY AND GET A MAINTENANCE WRITE OFF BEFORE DEP. GEAR WARNING CIRCUIT BREAKER HAD OPENED ON THE PREVIOUS FLT.
Narrative: UPON ARR INTO THE HOUSTON AREA WE STARTED OUR APCH. WHEN WE EXTENDED THE GEAR THERE WERE NO INDICATIONS OF THE 3 GEAR LIGHTS. WE NOTICED THAT THE GEAR INDICATOR LIGHT CB WAS POPPED OUT. THE COPLT RESET THE CB AND THE 3 GEAR LIGHTS WERE ILLUMINATED. WE FLEW BY THE TWR TO ENSURE THE GEAR WAS DOWN AND THEY INDICATED THAT IT WAS DOWN. AS A PRECAUTIONARY MEASURE I TOLD THE TWR TO HAVE THE FIRETRUCKS STANDING BY. WE CIRCLED THE ARPT AND LANDED WITH NO INCIDENT. ON THE GND, I CALLED MAINT AND WAS ON THE PHONE FOR APPROX 5 MINS. I WAITED UNTIL APPROX 5 MINS AFTER DEP TIME FOR A RETURN PHONE CALL. I DEPARTED THE ACFT TO AUSTIN AND NEGLECTED TO COM WITH MAINT. CONSIDERING THE PAX COMFORT AND COMPANY SCHEDULE, WE FLEW THE ACFT TO AUSTIN. SINCE THE ACFT SEEMED TO BE AIRWORTHY BEING THE ONLY THING WRONG WAS A CB THAT HAD POPPED OUT AND WAS RESET. THE ACFT ARRIVED IN AUSTIN AND THERE WAS NOTHING FOUND WRONG WITH IT. MAINT RELEASED THE ACFT AS AIRWORTHY.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.