37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 627645 |
Time | |
Date | 200408 |
Day | Mon |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | navaid : bxk.vortac |
State Reference | AZ |
Altitude | msl single value : 14000 |
Environment | |
Flight Conditions | VMC |
Weather Elements | Thunderstorm |
Aircraft 1 | |
Controlling Facilities | tracon : p50.tracon |
Operator | common carrier : air carrier |
Make Model Name | MD-80 Series (DC-9-80) Undifferentiated or Other Model |
Operating Under FAR Part | Part 121 |
Flight Phase | climbout : intermediate altitude |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
ASRS Report | 627645 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
ASRS Report | 627646 |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | aircraft equipment other aircraft equipment : #1 engine instruments other flight crewa other flight crewb |
Resolutory Action | flight crew : declared emergency flight crew : diverted to another airport flight crew : landed in emergency condition |
Consequence | other other |
Supplementary | |
Problem Areas | Aircraft |
Primary Problem | Aircraft |
Narrative:
On climb out from phoenix, at approximately 14000 ft, there was a loud bang as well as a yaw to the left as a result of an engine failure on the left engine. The engine failure QRH was accomplished, an emergency declared and we made an immediate return and landing in phoenix. Approach, landing and rollout were normal. An overweight landing at approximately 134000 pounds was made. Flight crew was debriefed and inquiries made as to whether any passenger required medical assistance. None was needed. We were unsure of what caused this failure. The engine has been replaced, and the damaged one will be torn down to determine the cause. Callback conversation with reporter revealed the following information: in talking to both rptrs, neither knows what, in the engine, failed. The crew inspected the engine after landing. There were numerous turbine blades damaged, as though something went through them. The air carrier replaced the engine.
Original NASA ASRS Text
Title: MD80 CREW HAD #1 ENG FAILURE DEPARTING PHX.
Narrative: ON CLBOUT FROM PHOENIX, AT APPROX 14000 FT, THERE WAS A LOUD BANG AS WELL AS A YAW TO THE L AS A RESULT OF AN ENG FAILURE ON THE L ENG. THE ENG FAILURE QRH WAS ACCOMPLISHED, AN EMER DECLARED AND WE MADE AN IMMEDIATE RETURN AND LNDG IN PHOENIX. APCH, LNDG AND ROLLOUT WERE NORMAL. AN OVERWT LNDG AT APPROX 134000 LBS WAS MADE. FLT CREW WAS DEBRIEFED AND INQUIRIES MADE AS TO WHETHER ANY PAX REQUIRED MEDICAL ASSISTANCE. NONE WAS NEEDED. WE WERE UNSURE OF WHAT CAUSED THIS FAILURE. THE ENG HAS BEEN REPLACED, AND THE DAMAGED ONE WILL BE TORN DOWN TO DETERMINE THE CAUSE. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: IN TALKING TO BOTH RPTRS, NEITHER KNOWS WHAT, IN THE ENG, FAILED. THE CREW INSPECTED THE ENG AFTER LNDG. THERE WERE NUMEROUS TURBINE BLADES DAMAGED, AS THOUGH SOMETHING WENT THROUGH THEM. THE ACR REPLACED THE ENG.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.